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Atlas / NTSB / ANC93LA053

NTSB CAROL · Event

Event ANC93LA053

1993-04-23 GOOSE BAY, Alaska, United States Airport · Z40 None 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

THE INSTRUCTOR PILOT'S DELAY OF REMEDIAL ACTION DURING THE SIMULATED FORCED LANDING. FACTORS WERE THE DUAL STUDENT'S FAILURE TO MAINTAIN THE PROPER DESCENT RATE, AND HIS FAILURE TO ATTAIN PROPER ALIGNMENT WITH THE RUNWAY PRIOR TO TOUCHDOWN.

Factual narrative

WHILE ON THE DOWNWIND PORTION OF THE TRAFFIC PATTERN THE CFI INITIATED A SIMULATED ENGINE FAILURE. HE AND THE COMMERCIAL STUDENT PILOT STATED THAT JUST BEFORE TOUCHDOWN THE AIRPLANE'S RATE OF DESCENT INCREASED RAPIDLY. THE APPLICATION OF ENGINE POWER DID NOT ARREST THE RATE OF DESCENT BEFORE THE AIRPLANE LANDED HARD. THE AIRPLANE'S LEFT WING HIT THE GROUND FIRST, FOLLOWED BY THE LEFT MAIN LANDING GEAR. BOTH PILOTS STATED THAT AT THE TIME OF TOUCHDOWN THE AIRPLANE WAS IN AN APPROXIMATE 5 DEGREE LEFT BANK. THE LEFT MAIN LANDING GEAR SEPARATED AND THE LEFT WING HIT THE GROUND. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1993_ANC93LA053.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (engine failure). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗