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Atlas / NTSB / ATL04LA034

NTSB CAROL · Event

Event ATL04LA034

2003-11-07 Birmingham, Alabama, United States Airport · BHM None 1 aircraft Status: Completed

Registry · N1015T

FAA Aircraft Registry record.

Make / Model

DIAMOND AIRCRAFT DA 40 NG

Year of manufacture

2021

Engine

AUSTRO E4-A (168 hp)

Seats / Engines

5 seats · 1 engine

Last airworthiness date

20211015

ADS-B equipped

Yes — Mode-S A00B84

Registrant of record

HARRIS NAIL INVESTMENTS LLC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The certified flight instructor's inadequate aircraft control and his improper landing flare resulting in a hard landing and roll over.

Factual narrative

On November 7, 2003, at 1715 central standard time, a Hughes 269A, N1015T, registered to Hoverwork Helicopters Inc., operated by Liberty Flight Center, as a 14 CFR Part 91 instructional flight, collided with the ground next to taxiway "B", at the Birmingham International Airport, Birmingham, Alabama, while on approach to a hover. Visual meteorological conditions prevailed and no flight plan was filed. The helicopter received substantial damage. The commercial pilot flight instructor (CFI) and commercial pilot receiving instruction reported no injuries. The flight originated from Birmingham International Airport on November 7, 2003, at 1710. The CFI stated a preflight inspection was conducted and no anomalies were noted. They entered the helicopter, conducted the required checks, started the helicopter, and contacted Birmingham Tower for taxi clearance. They received clearance to hover to the sod area located in the vicinity of taxiway "B". The pilot receiving instruction initiated the hover and hovered to the sod area at 50 feet. The rotor rpm was in the green and the manifold pressure indicated 25 inches. The landing light was not used. The pilot receiving instruction started his descent over the sod area and planned to come to a 3-foot hover. The rotor rpm remained in the green and manifold pressure was decreased to 20 inches. The pilot receiving instruction continued the descent down to about 5 feet. The CFI stated the ground was coming up and the manifold pressure was still at 25 inches. The CFI took over the flight controls with the other pilot, and increased the throttle, but there appeared to be no response. The CFI leveled the helicopter and it collided with the ground in a level attitude. Everything appeared to be ok, but it felt like something gave way or broke on the airframe. The CFI increased collective pitch and was able to hold the helicopter level for about 3 to 4 seconds before it rolled over on its left side. Examination of the helicopter after they exited revealed the cross tubes on the left side had broken. Examination of the crash site revealed the left skid of the helicopter dug into the ground on a 45-degree angle clockwise to the flight path. The left skid collapsed, and the cross tube support brackets were broken. The right skid was intact. The helicopter rolled over on its left side. All three main rotor blades were damaged and tail boom separated. A compression test was performed on all engine cylinders. The compression was 70/80 on all cylinders except for cylinder 4. The compression on the No. 4 cylinder was 21/80. The student pilot was making an approach for landing. The certified flight instructor noticed the ground was getting closer and the manifold pressure indicated 25 inches. The flight instructor took over the flight controls and increased the throttle, but there appeared to be no response. The flight instructor stated he leveled the helicopter and collided with the ground in a level attitude and the helicopter rolled over on it's left side. Examination of the crash site revealed the helicopter collided with the ground left skid low at a 45-degree angle to the flight path. The left skid collapsed, the cross tube support brackets were broken, and the right skid was intact. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2003_ATL04LA034.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.