NTSB CAROL · Event
Event CEN12LA384
Registry · N76NP
FAA Aircraft Registry record.
Make / Model
PETERSON-FEDER-SPLINTER STARDUSTER TOO
Engine
LYCOMING O&VO-360 SER (180 hp)
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19820529
ADS-B equipped
Yes — Mode-S AA4069
Registrant of record
COLLINS SHANNAN S
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
A partial loss of engine power on takeoff due to a stuck intake valve on the No. 2 cylinder.
Factual narrative
On June 15, 2012, at 1945 central daylight time, N76NP, an amateur built-experimental Stolp Starduster SA-300 airplane, sustained substantial damage when it made a forced landing to a canal after a partial loss of engine power shortly after takeoff from Lakeview Airport (30F), Lake Dallas, Texas. The airline transport pilot and the passenger sustained minor injuries. The airplane was registered to and operated by a private individual. Visual meteorological conditions prevailed and no flight plan was filed for the local pleasure flight conducted under 14 Code of Federal Regulations Part 91. The pilot stated that he performed a preflight inspection of the airplane and confirmed there were 12.5 gallons of fuel in the fuel tank, which was enough for a 1 hour and 20 minute flight. After finding no anomalies during the preflight; engine start, and engine run-up, the pilot and his passenger departed for a 15 minute flight around Lake Lewisville before returning to the airport. The pilot made a low pass over runway 18R before he re-entered the traffic pattern and made a touch and go landing. During climb-out, at an altitude of approximately 100 feet above the ground, the engine began "producing less than full power." The pilot quickly verified the throttle was full forward; the mixture was rich, and the carburetor heat was the full forward (cold) position. It was also at this time, that he began to smell unburned fuel. The pilot was unable to maintain altitude and prepared for a landing straight ahead, but there was a crowded marina. The pilot elected to make a left hand turn away from the marina knowing that the airplane would most likely stall. The airplane stalled, the left wing dropped, and the airplane impacted the water in a 45 to 90 degree nose down angle. The pilot said the engine was still running when they hit the water but at a reduced RPM. The airplane was recovered from the water approximately 2.5 hours after the accident and placed in the owner's hanger. According to the pilot,the gascolator was bent and leaking fuel. He also said the lower and upper left wings, and lower right wing had spar and rib damage. The airplane owner performed an examination of the engine and said the engine was rotated using the starter via the ignition switch. When the engine was rotated, the mechanical fuel pump was observed pumping fuel; however, due to water damage the magnetos did not spark. The fuel line to the mechanical fuel pump was removed and fuel was found in the line. The carburetor was removed and disassembled. The bowl was full of water. A compression check was successful on each cylinder except the #2 cylinder (#1-74 psi, #2-20 psi, #3-70 psi, and #4-70 psi). Removal of the #2 cylinder revealed the intake valve was stuck in the open position. The pilot held an airline transport pilot rating for airplane multi-engine land. In addition, he held an airplane single-engine sea rating and an airframe and powerplant certificate. The pilot's last Federal Aviation Administration (FAA) First Class medical was issued on March 7, 2012. He reported a total of 11,250 total hours, of which, 40 hours were in the accident airplane. Shortly after takeoff, the airplane's engine lost partial power. The pilot was unable to maintain altitude, so he elected to perform a forced landing. He turned the airplane to the left to avoid a crowded marina, and the airplane stalled and impacted the water. Examination of the engine revealed that the No. 2 cylinder's intake valve was stuck in the open position. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Failure - C
Verbatim from NTSB's published report. Source file
NTSB_2012_CEN12LA384.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
Beyond the agency record
Search this event elsewhere.
Pre-filled searches into the sources where news + community discussion of aviation events lives. External sources are reported, not agency. Treat them as signal that something happened, not as fact about what happened.
Entity-clustered aviation events in the press — last 24 hr + 30-day archive.
Official agency record + docket.
Investigative docket: factual reports, photos, transcripts.
Long-running aviation incident database (Flight Safety Foundation).
Community NTSB synthesis blog — often has photos and witness reports.
Gold-standard aviation incident blog.
Aviation industry news search.
GA pilot forum — informed but rumor-prone.
GA pilot subreddit search.
Tail-number page — flight history (free tier limited).
AOPA Air Safety Institute search.
Mainstream press coverage. Recent events only.
Privacy-preserving news search.
External links open in a new tab. We don't ingest their content; we deep-link search queries.
Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2026 · Conference Paper
Computational Analysis of Steady State Aerodynamics of Transonic Truss-Braced Wing Configuration in Deep Stall
This study presents a computational investigation of steady state aerodynamics of the Subsonic Ultra-Green Aircraft Research (SUGAR) Transonic Truss-Braced Wing (TTBW) configuration over a wide range …
- arXiv 2023 · arXiv preprint
Automating Bird Diverter Installation through Multi-Aerial Robots and Signal Temporal Logic Specifications
This paper tackles the task assignment and trajectory generation problem for bird diverter installation using a fleet of multi-rotors.
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- arXiv 2023 · arXiv preprint
Polycrystallinity enhances stress build-up around ice
Damage caused by freezing wet, porous materials is a widespread problem, but is hard to predict or control. Here, we show that polycrystallinity makes a great difference to the stress build-up process…
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- Embry-Riddle Scholarly Commons 2021 · Journal article (JAAER)
Analysis on the Negative Emotional, Physiological, and Cognitive Responses Elicited from of the Activation of a Stall Alarm
Failing to identify an aerodynamic stall can lead to the inability of an aircraft to sustain flight. To warn pilots of an impending or fully-developed stall, many aircraft have safety devices installe…
Browse the full corpus — academia portal ↗