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Atlas / NTSB / CHI99LA339

NTSB CAROL · Event

Event CHI99LA339

1999-09-12 ANN ARBOR, Michigan, United States Serious 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The pilot's improper touchdown during a water landing.

Factual narrative

On September 12, 1999, at 1327 eastern daylight time, a Lake LA-4, N1137L, sustained substantial damage during a landing on Bruin Lake, about 18 miles northwest of Ann Arbor, Michigan. The airline transport rated pilot received serious injuries. The personal 14 CFR Part 91 flight was operating in visual meteorological conditions. No flight plan was on file. The local flight departed Pontiac, Michigan, about 1300. The pilot told police authorities that he was going to practice a touch and go landing on the lake. He said that on touchdown the airplane decelerated as if "the brakes were locked." The pilot said he did not know what caused the accident. The pilot did not indicate any mechanical problem with the airplane. Subsequent to the accident an examination of the wreckage was conducted. The Federal Aviation Administration inspector said the airplane was broken into three major pieces and was recovered from the lake the day following the accident. He said his examination of the wreckage failed to reveal any pre-impact anomalies. He said landing gear was in the retracted position. He said that when he talked to police authorities they told him, "According to witnesses [the pilot] was attempting a landing on Bruin Lake when he lost control of the aircraft. One of the sponsons hit the water causing the aircraft to flip." The pilot told police he was going to practice a touch and go landing on the lake. He said that on touchdown the airplane decelerated as if 'the brakes were locked,' and the airplane cartwheeled. The pilot did not indicate any mechanical problem with the airplane. Subsequent to the accident an examination of the wreckage was conducted. The inspector said the airplane was broken into three major pieces. He said his examination of the wreckage failed to reveal any pre-impact anomalies. He said landing gear was in the retracted position. He said that when he talked to police authorities they told him, 'According to witnesses [the pilot] was attempting a landing on Bruin Lake when he lost control of the aircraft. One of the sponsons hit the water causing the aircraft to flip.' Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1999_CHI99LA339.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.