NTSB CAROL · Event
Event ERA11LA519
Aircraft involved
Probable cause & findings
The non-certificated pilot's improper flare on an earlier flight, which resulted in a hard landing, fracture of the right main landing gear bolt, and subsequent collapse of the right main landing gear.
Factual narrative
On September 19, 2011, about 0930 eastern daylight time, an experimental amateur-built Heinlein GH125, N79GH, was substantially damaged when the right main landing gear collapsed during landing roll at Okeechobee County Airport (OBE), Okeechobee, Florida. The non-certificated pilot was not injured. The airplane was registered to the pilot and operated under 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed, and no flight plan was filed for the local personal flight, which originated at OBE. After landing and while taxiing to the ramp area, the right main landing gear collapsed, the airplane turned 180 degrees, and came to rest on the runway. The right wing was substantially damaged during the accident sequence. A post accident examination of the main landing gear by the pilot revealed that a bolt in the right main landing gear had fractured. The pilot, age 72, had previously held a student pilot certificate which expired in 2003. His most recent FAA third-class medical certificate was issued in June of 2001. He reported 300 total flight hours, of which, 70 hours were in the same make and model as the accident airplane. In addition, he reported that he had flown 5 hours in the last 30 days. According to FAA records, the airplane was manufactured in 1993, and registered to the pilot in 2007. It was a two-seat, high-wing monoplane, which had conventional tailwheel landing gear. It was equipped with a Lycoming O-290 series, 130-horsepower engine. The most recent condition inspection was performed on September 28, 2010, by the pilot, who did not hold a repairman certificate for the airplane. The right main landing gear bolt was examined by the Safety Board Materials Laboratory. According to the Laboratory's factual report, based on the deformation of the bolt shank and the fracture surface features, the bolt fractured in overstress due to concomitant shear and bending stresses. According to the pilot, the right main landing gear bolt had accumulated 265 hours of total time in service. In addition, he stated that he might have landed the airplane "hard" on the day of the accident and also a few times prior to the accident. The non-certificated pilot was taxiing the airplane to the ramp area when the right main landing gear collapsed. The airplane rotated 180 degrees, damaging the right wing before coming to rest. A postaccident examination revealed that a bolt in the right main landing gear had fractured. Subsequent examination of the bolt determined that it fractured in overstress due to concomitant shear and bending stresses. In addition, the pilot stated that he might have landed the airplane hard on the day of the accident and also a few times prior to the accident. The right main landing gear bolt had accumulated 265 hours of total time in service. No additional mechanical anomalies were noted with the airplane. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Landing flare-Not attained/maintained - C
- C Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
Verbatim from NTSB's published report. Source file
NTSB_2011_ERA11LA519.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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