NTSB CAROL · Event
Event ERA20LA006
Registry · N166HJ
FAA Aircraft Registry record.
Make / Model
HONDA AIRCRAFT CO LLC HA-420
Year of manufacture
2017 · 2 years old at event
TCDS
A00018AT · HONDA AIRCRAFT COMPANY LLC
Engine
GE HONDA HF-120
Seats / Engines
8 seats · 2 engines
Last airworthiness date
20170727
ADS-B equipped
Yes — Mode-S A108B0
Registrant of record
REGISTRATION PENDING
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
Ground personnel’s use of an improper towbar adapter lug, which prevented the nose landing gear from extending.
Factual narrative
On October 7, 2019, about 0830 eastern daylight time, a Honda, HA-420, H166HJ, was substantially damaged when it was involved in an accident near Charleston, South Carolina. The airline transport pilot and four passengers were not injured. The airplane was operated by Pro by Air, as a Title 14 Code of Federal Regulations Part 91 executive/corporate flight. The pilot stated that, during the landing approach, he moved the landing gear handle to the DOWN position. The main landing gear indicator was green, but the nose landing gear indicator was yellow; followed by an unsafe audible alarm indicating that the gear was unsafe. The pilot aborted the approach and requested a tower flyby, during which the tower reported that the, “doors did not look right.” The pilot attempted to cycle the gear twice, but was not able to resolve the issue. The pilot declared an emergency and performed the emergency gear extension checklist, after which the gear lights indicated that the two main landing gear were extended and locked; however, the nose landing gear indicator light was red. After performing the emergency gear extension, the pilot received a warning message about the gear doors. The pilot performed a normal approach and landing and the airplane slid to a complete stop on the runway. The pilot and all passengers deplaned on the runway and waited for emergency services. An examination of the airplane by a Federal Aviation Administration inspector revealed substantial damage to the fuselage. Further examination revealed that the pressure vessel was damaged as a result of the gear-up landing. The airplane was recovered to a hangar for further examination by the FAA and representatives of the Honda Aircraft Company. A towbar adapter lug was discovered inside of the nose wheel axle assembly. The towbar adapter lug was removed, and the length and width dimensions of the adapter lug was documented along with its part number (P228). The adapter lug was compared to the chart of the original equipment manufacturer (OEM), Brackett Aircraft Company Inc. The adapter lug was not a Honda Aircraft part, nor was it the OEM specified lug for the accident airplane. A witness mark was discovered on the top surface of the door and at the bottom of the nose landing gear bay. The clearance between the nose landing gear door and the nose landing gear axle without the discovered adapter lug inserted measured approximately 11/16-inch. The adapter lug was reinserted into the nose wheel gear axle assembly with approximately 1.5 inches of the adapter lug extending from the axle assembly. There was a considerable negative clearance between the fuselage and the adapter lug. A representative for the fixed based operator (FBO) who performed ground handling on the airplane stated that they use pin adapters when connecting the nose wheel to the towbar, because the wheel hubs are too small for the universal towbar hookup. The pilot stated that, during the landing approach, after extending the landing gear, he received a yellow nose landing gear indicator light and an aural “gear unsafe” warning. He aborted the approach to troubleshoot and, after performing an emergency gear extension, received a red nose landing gear light and a warning message indicating a problem with the landing gear doors. The pilot subsequently landed and the airplane settled onto the nose, resulting in substantial damage to the fuselage. Examination of the airplane revealed a towbar adapter lug inside of the nose wheel axle assembly. The adapter lug was not a produced by the airplane manufacturer nor was it specified for use for the accident airplane. A witness mark was discovered on the top surface of the nose landing gear door and at the bottom of the nose landing gear bay. It is likely that, based on the incorrect size of the towbar adapter lug, the nose wheel landing gear became stuck in the stowed/retracted position. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- — Personnel issues-Action/decision-Action-Incorrect action performance-Ground crew
- — Aircraft-Aircraft systems-Landing gear system-Nose/tail landing gear-Malfunction
Verbatim from NTSB's published report. Source file
NTSB_2019_ERA20LA006.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
Beyond the agency record
Search this event elsewhere.
Pre-filled searches into the sources where news + community discussion of aviation events lives. External sources are reported, not agency. Treat them as signal that something happened, not as fact about what happened.
Entity-clustered aviation events in the press — last 24 hr + 30-day archive.
Official agency record + docket.
Investigative docket: factual reports, photos, transcripts.
Long-running aviation incident database (Flight Safety Foundation).
Community NTSB synthesis blog — often has photos and witness reports.
Gold-standard aviation incident blog.
Aviation industry news search.
GA pilot forum — informed but rumor-prone.
GA pilot subreddit search.
Tail-number page — flight history (free tier limited).
AOPA Air Safety Institute search.
Mainstream press coverage. Recent events only.
Privacy-preserving news search.
External links open in a new tab. We don't ingest their content; we deep-link search queries.