NTSB CAROL · Event
Event IAD02LA092
Registry · N7223R
FAA Aircraft Registry record.
Make / Model
GLASAIR GLASAIR
Year of manufacture
1997 · 5 years old at event
Engine
LYCOMING I0360 SER (180 hp)
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19970801
ADS-B equipped
Yes — Mode-S A9ADCB
Registrant of record
LIVELY CHARTERS INC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The pilot's improper positioning of the throttle during engine start, which resulted in his inability to maintain control of the airplane.
Factual narrative
On September 6, 2002, at 1430 eastern daylight time, a homebuilt Glassair, N7223R, was substantially damaged during an engine start at Minuteman Airfield (6B6), Stow, Massachusetts. The certificated private pilot was not injured. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight that was to be conducted under 14 CFR Part 91. According to the pilot, he set the vernier-type throttle to "a little more than 1/4-inch open," and started the airplane. He then attempted to reduce the power by twisting the throttle counter-clockwise. However, he was unable to retard the throttle to the idle position. The brakes could no longer hold the airplane, and it began to move forward and turn to the left. As the pilot again tried to reduce the power, the airplane went through a fence and came to rest as it impacted a parked car. The pilot also stated that he forgot about the center lock button on the throttle and did not notice that it was engaged during the engine start sequence. He stated the accident was due to "pilot error." Examination of the airplane by a Federal Aviation Administration (FAA) inspector revealed that the throttle was closed, and the mixture control was in the idle-cutoff position. A functional test of the throttle was performed and no anomalies were noted. Additionally, no brake or skid marks were observed on the pavement or the grass. The pilot reported that he had accumulated 1,500 hours of total flight experience, 10 of which were in make and model. The pilot stated that he set the vernier-type throttle to "a little more than 1/4-inch open," and started the airplane. He attempted to reduce power by twisting the throttle counter-clockwise, but was unable to retard the throttle to the idle position. The brakes could no longer hold the airplane, which moved forward, turned to the left, went through a fence and came to rest as it impacted a parked car. The pilot stated that he forgot about the center lock button on the throttle and did not notice that it was engaged during the engine start sequence. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2002_IAD02LA092.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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