Skip to content

Atlas / NTSB / LAX91LA402

NTSB CAROL · Event

Event LAX91LA402

1991-09-21 BUCKEYE, Arizona, United States Airport · BXK Minor 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

THE PASSENGER/CERTIFIED FLIGHT INSTRUCTOR'S POOR JUDGEMENT BY INTERFERING WITH THE PIC AND HIS FAILURE TO EXECUTE A TIMELY GO-AROUND. CONTRIBUTING TO THIS ACCIDENT WAS THE CFI'S MISJUDGMENT OF ALTITUDE.

Factual narrative

WHEN THE FLT ARRIVED AT ITS DESTINATION AIRPORT, THE PASSENGER, A CFI, SUGGESTED TO THE PIC, A PRIVATE PILOT, THAT HE PRACTICE A SIMULATED ENGINE OUT APPROACH/LANDING. THE PIC THROTTLED BACK THE ENGINE UPON ENTERING THE LEFT DOWNWIND LEG. WHEN ON FINAL APPROACH WITH FULL FLAPS EXTENDED, THE PIC REALIZED THE ACFT WAS TOO HIGH AND BEGAN TO SLIP THE AIRPLANE. WHEN NEARING THE THRESHOLD THE ACFT WAS STILL TOO HIGH AND THE PAX (CFI) ASSUMED THE CONTROLS AND ENTERED A 360 DEGREE TURN. DURING THE TURN THE CFI REALIZED THE AIRPLANE WAS TOO LOW AND APPLIED POWER TO GO AROUND, BUT TO NO AVAIL. THE AIRPLANE STRUCK THE GROUND AND CARTWHEELED. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1991_LAX91LA402.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (go-around). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗