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Atlas / NTSB / MIA91LA189

NTSB CAROL · Event

Event MIA91LA189

1991-07-20 HILLIARD, Florida, United States Airport · 01J Minor 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

LOSS OF ENGINE POWER DUE TO UNDETERMINED REASONS, FAILURE OF THE PILOT TO MAINTAIN VSO, AND INADVERTENT STALL MUSH. CONTRIBUTING TO THE ACCIDENT WAS LACK OF TOTAL EXPERIENCE IN THE TYPE OF OPERATION.

Factual narrative

THE PLT STATED THAT SHORTLY AFTER TAKEOFF, THE ACFT WAS NOT CLIMBING PROPERLY AND THE LT WING DROPPED. THE ACFT THEN COLLIDED WITH TREES AND THE GROUND. THE ENG WAS REMOVED AND PLACED ON A TEST STAND FOR AN OPERATIONAL TEST. THE ENG STARTED AND OPERATED TO NEARLY FULL STATIC RPM WITH NO MALFUNCTIONS NOTED. THE ACFT'S FLT CONTROLS WERE EXAMINED BY AN FAA AIRWORTHINESS INSPECTOR AND FOUND TO BE FREE OF PREIMPACT FAILURE OR MALFUNCTION. THE STALL WARNING HORN WAS TESTED AND OPERATED NORMALLY. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1991_MIA91LA189.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗