NTSB CAROL · Event
Event MIA95LA138
Registry · N28FE
FAA Aircraft Registry record.
Make / Model
BOMBARDIER INC BD-100-1A10
Year of manufacture
2012
TCDS
T00005NY · BOMBARDIER INC
Engine
HONEYWELL AS907-1-1A
Seats / Engines
8 seats · 2 engines
Last airworthiness date
20120405
ADS-B equipped
Yes — Mode-S A2CC24
Registrant of record
FEDERAL EXPRESS LEASING CORP
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
LOSS OF ENGINE POWER DUE TO SEPARATION OF 3 CONNECTING RODS FROM THE MASTER ROD FOR UNDETERMINED REASONS(S).
Factual narrative
On May 28, 1995, about 1340 eastern daylight time, a North American T-28A, N28FE, registered to the Park Avenue Group, was substantially damaged during a forced landing near Arcadia, Florida, while on a 14 CFR Part 91 personal flight. Visual meteorological conditions prevailed at the time and no flight plan was filed. The airline transport-rated pilot, the sole occupant, was not injured. The flight originated from the Peter O'Knight Airport, Tampa, Florida, about 1325. The pilot stated that while climbing through 2,500 feet he observed the oil temperature increase and the oil pressure decrease. He then initiated a descent for a forced landing and intentionally landed gear-up in a field. The engine was removed for further examination. Examination of the engine by an FAA airworthiness inspector revealed that the cylinder Nos. 4, 5, and 6 connecting rods were separated from the master rod for undetermined reason(s). Review of the engine logbook revealed that the engine was overhauled on July 25, 1994. The total time on the engine at the time of overhaul was about 5,347 hours. The engine had accumulated about 18 hours since overhaul at the time of the accident. THE PILOT STATED THAT AFTER TAKEOFF WHILE CLIMBING THROUGH 2,500 FEET, THE OIL PRESSURE BEGAN DROPPING AND THE OIL TEMPERATURE BEGAN INCREASING. HE EXECUTED A FORCED LANDING IN A COW PASTURE LANDING INTENTIONALLY GEAR-UP. EXAMINATION OF THE ENGINE REVEALED THAT 3 CONNECTING RODS WERE SEPARATED FROM THE MASTER ROD FOR UNDETERMINED REASON(S). REVIEW OF THE ENGINE LOGBOOK REVEALED THAT THE ENGINE WAS OVERHAULED ON JULY 25, 1994. THE TOTAL TIME ON THE ENGINE AT THAT TIME WAS 5,347 HOURS AND THE ENGINE HAD ACCUMULATED ABOUT 18 HOURS SINCE OVERHAUL AT THE TIME OF THE ACCIDENT. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_1995_MIA95LA138.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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