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Atlas / NTSB / SEA95LA153

NTSB CAROL · Event

Event SEA95LA153

1995-07-17 OGDEN, Utah, United States Airport · OGD None 1 aircraft Status: Completed

Registry · N6953K

FAA Aircraft Registry record.

Make / Model

PIPER PA-20

Seats / Engines

4 seats · 1 engine

ADS-B equipped

Yes — Mode-S A94014

Registrant of record

JESSUP ROBERT L

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

THE PILOT-IN-COMMAND'S FAILURE TO MAINTAIN DIRECTIONAL CONTROL. HTE LOOSE TAILWHEEL ASSEMBLY BOLT WAS A FACTOR.

Factual narrative

On July 17, 1995, at 1935 mountain daylight time, a Piper PA-20, N6953K, ground looped after landing at the Ogden Airport, Ogden, Utah. Visual meteorological conditions prevailed at the time and no flight plan was filed for the local instructional flight. The airplane was substantially damaged and the flight instructor and student pilot were not injured. During a telephone interview and subsequent written statement, the flight instructor stated that this was his first flight with this student pilot who was preparing to take the private pilot check ride. The student pilot was at the controls for takeoff and the flight stayed in the pattern to practice touch-and-go landings. During the first approach, the flight instructor stated that he took control of the airplane on final approach to demonstrate a procedure to the student. After a three point touchdown, the flight instructor noticed a strange noise and felt a vibration that he couldn't pin down. The flight instructor thought that it may be a flat main landing gear as he was having to input more left rudder control to maintain runway centerline. As the airplane slowed to 10 to 15 knots, the flight instructor stated that he was unable to maintain directional control as the nose of the airplane veered to the right and the airplane ground looped. A Federal Aviation Administration Inspector from the Salt Lake City, Utah, Flight Standards District Office, inspected the airplane and found that the tailwheel pivot bolt was loose, which resulted in the tailwheel shimmy during the landing roll. The airframe and engine logbooks indicate that the last annual inspection was performed on 12/16/93. The logbooks list several major repairs and alterations since 12/7/93. THE FLIGHT INSTRUCTOR STATED THAT HE HEARD A STRANGE NOISE AND FELT A VIBRATION DURING THE LANDING ROLL. HE THOUGHT THAT IT MIGHT BE A FLAT MAIN LANDING GEAR TIRE AS HE WAS HAVING TO INPUT MORE LEFT RUDDER CONTROL TO MAINTAIN RUNWAY CENTERLINE. AS THE AIRPLANE SLOWED, THE CFI WAS UNABLE TO MAINTAIN DIRECTIONAL CONTROL AS THE NOSE VEERED TO THE RIGHT AND THE AIRPLANE GROUND LOOPED. DURING THE POST CRASH INSPECTION, THE TAILWHEEL PIVOT BOLT WAS FOUND TO BE LOOSE. REVIEW OF THE AIRCRAFT LOGBOOKS INDICATE THAT IT HAD BEEN 19 MONTHS SINCE THE LAST ANNUAL INSPECTION. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1995_SEA95LA153.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.