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Atlas / NTSB / WPR12LA075

NTSB CAROL · Event

Event WPR12LA075

2012-01-05 Las Vegas, Nevada, United States Airport · VGT None 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The pilot's failure to maintain directional control of the airplane during the landing roll.

Factual narrative

On January 5, 2012, at 1539 Pacific standard time, a Piper Aerostar 601P, N104RM, sustained substantial damage during a landing at North Las Vegas Airport (VGT), Las Vegas, Nevada. The private pilot, the sole occupant of the airplane, was not injured. The owner/pilot was operating the airplane under the provisions of 14 Code of Federal Regulations Part 91. Visual meteorological conditions prevailed for the personal local flight, which had originated approximately 39 minutes before the accident. A flight plan had not been filed. The pilot stated that the purpose of the flight was to practice instrument landing approaches. On the third approach, he requested to side step from runway 12 left to 12 right for a full stop landing. The tower controller approved the side step and cleared him for landing. The pilot reported that almost immediately after touchdown, the airplane began “wavering” and moments later, veered to the left. He attempted to regain directional control with the application of “full right rudder” and subsequently the airplane departed the right side of the runway. The pilot attributed the loss of directional control to a main landing gear malfunction. A witness said that the airplane’s landing touchdown was “firm” but not abnormal. Several witnesses observed the airplane to “fishtail” almost immediately after touchdown and drift towards the left side of the runway. As the airplane approached the left side of the runway, it “yawed” right and went “skidding” down the runway while facing right. The left engine propeller blades began contacting the runway. The witness said that as the airplane began moving to the right side of the runway, he heard the right engine increase to near full power. When the airplane entered the dirt on the right side of the runway, it spun to the left coming to rest facing the opposite direction from its approach to landing. Postaccident inspection of the airplane by a Federal Aviation Administration (FAA) inspector revealed that both wings were bent up, the wing flaps were bent, the left wing’s fuel tank was compromised, and the fuselage had several holes in it. On January 25, 2012, the airplane was examined by the FAA inspector and a licensed mechanic. They found the left propeller assembly feathered, and the right propeller blades were bent forward. Examination of the cockpit revealed the both throttle leavers were in the aft/closed position, the propeller control leavers were full forward, and the mixture controls were full rich. The throttle levers in the cockpit exhibited normal operation and friction, but both propeller control levers exhibited little friction and could be moved with one finger’s pressure. The pilot had not reported any malfunctions with the airplane’s engines or their propeller assemblies. A police video documented that moments after the accident, a police officer suggested that the pilot turn the airplane's electrical power off; the pilot was observed to reenter the accident airplane. The mechanic suggested that the forward bending of the right propeller blades indicated that the right engine was at a high power setting when it contacted the ground and that the airplane was sliding backwards. Additional, the right wing flaps were bent forward indicating aft movement at the time of terrain contact. The airplane’s nose and main landing gears were examined, and no preimpact anomalies were identified. The pilot reported that, immediately after touchdown, the airplane began “wavering” and moments later veered to the left. He attempted to regain directional control with the application of “full right rudder” and the airplane subsequently departed the right side of the runway. A witness reported that the airplane’s touchdown was “firm” but not abnormal. As the airplane approached the left side of the runway, it yawed right and skidded down the runway while facing right. As the airplane began moving to the right side of the runway, the witness heard the right engine increase to near full power. The airplane spun to the left, coming to rest facing the opposite direction from its approach to landing. Another witness reported seeing the propellers contact the ground. The pilot attributed the loss of directional control to a main landing gear malfunction. Postaccident examination of the airplane revealed that the left propeller assembly was feathered and that the right propeller blades were bent forward, indicative of the right engine impacting terrain under high power. Both throttle levers were found in the aft/closed position, and both propeller control levers were in the full-forward position. The propeller control levers exhibited little friction and could be moved with pressure from one finger. The evidence suggested that the pilot inadvertently feathered the left propeller assembly during the accident sequence. The pilot did not report any preaccident malfunctions or failures with the airplane’s engines or propeller assemblies that would have precluded normal operation. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • C Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
  • C Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Directional control-Not attained/maintained - C

Verbatim from NTSB's published report. Source file NTSB_2012_WPR12LA075.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.