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Atlas / NTSB / WPR20LA288

NTSB CAROL · Event

Event WPR20LA288

2020-08-26 Chino, California, United States Airport · CNO None 1 aircraft Status: Completed

Registry · N9540T

FAA Aircraft Registry record.

Make / Model

CESSNA 210

Year of manufacture

1960 · 60 years old at event

TCDS

3A21 · TEXTRON AVIATION INC

Engine

CONT MOTOR I0-470 SERIES (260 hp)

Seats / Engines

4 seats · 1 engine

ADS-B equipped

Yes — Mode-S AD45ED

Registrant of record

CHINO AVIATION INC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The failure of the engine-driven hydraulic pump, which resulted in the main landing gear not fully extending and locking into place during landing. Contributing to the accident was the failure of the emergency gear extension system for reasons that could not be determined.

Factual narrative

On August 26, 2020, about 0815 Pacific daylight time, a Cessna 210, N9540T, was substantially damaged when it was involved in an accident near Chino, California. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that the accident flight was the first flight since the airplane had undergone landing gear maintenance. While in the airport traffic pattern, he extended the landing gear; however, he noticed that it would not lock into the down position despite multiple attempts to cycle the landing gear, which included using the emergency landing gear extension procedure. The pilot said that he by twisted the landing gear extension handle to the left to unlock, pulled the handle out, and pumped it vertically up and down about 50 times with zero resistance. The pilot was unable to obtain a positive down and locked indication. The pilot stated that during landing on runway 26R, both main landing gear collapsed, the left wing and left horizontal stabilizer impacted the runway surface, and the airplane came to rest upright on the runway. Postaccident examination of the airplane by a Federal Aviation Administration inspector revealed that the left horizontal stabilizer and elevator were substantially damaged. Subsequent examination of the landing gear revealed that the landing gear power pack fluid level was about 12 ounces low from full, and the engine-driven hydraulic pump was not operational. No issues were noted with the emergency gear extension system. The airplane was placed on jacks and a hydraulic mule was attached to the hydraulic system. The landing gear extended and locked in place normally. The landing gear was retracted, and the emergency landing gear extension system was operated, and the landing gear extended and locked into place. The engine-driven hydraulic pump was removed from the engine, and the crankshaft was rotated by hand using the propeller. No evidence of any mechanical damage was observed to the engine accessory case. A visual inspection of the hydraulic pump revealed a torn section of a seal that surrounded the pump drive shaft. Further examination of the engine-driven hydraulic pump at a repair facility revealed that the load spring was misshaped, and the oil seal was hard, brittle, and torn, which resulted in an oil leak and the pump unable to hold pressure. The pilot reported that the accident flight was the first flight since the airplane had undergone recent landing gear maintenance. While in the airport traffic pattern, he extended the landing gear; however, he noticed that it would not lock into the down position. Despite multiple attempts to cycle the landing gear, which included using the emergency landing gear extension procedure, he was unable to obtain a positive down and locked indication. While landing, both main landing gear collapsed and the left wing and left horizontal stabilizer impacted the runway surface, which resulted in substantial damage to the left elevator and horizontal stabilizer. Postaccident examination of the airplane revealed that the engine-driven hydraulic pump was not operational. No mechanical damage was observed within the engine’s accessory case. No evidence of any preexisting mechanical malfunction was observed with the airframe or emergency gear extension system. Examination of the engine-driven hydraulic pump revealed a torn section of an oil seal that surrounded the pump drive shaft. The oil seal was hard, brittle, and torn, which resulted in an oil leak that prevented the pump from holding pressure, which likely prevented the landing gear from fully extending and locking into place during landing. The reason for the emergency gear extension system not functioning could not be determined. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft systems-Hydraulic power system-Pump, main-Damaged/degraded
  • Not determined-Not determined-(general)-(general)-Unknown/Not determined
  • Aircraft-Aircraft systems-Landing gear system-Gear extension and retract sys-Inoperative

Verbatim from NTSB's published report. Source file NTSB_2020_WPR20LA288.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗