Skip to content

Atlas / NTSB / BFO87FA048

NTSB CAROL · Event

Event BFO87FA048

1987-07-18 SALUDA, Virginia, United States Airport · W75 None 1 aircraft Status: Completed

Registry · N1810E

FAA Aircraft Registry record.

Make / Model

AERONCA 7AC

Year of manufacture

1946 · 41 years old at event

Engine

CONT MOTOR A&C65 SERIES (65 hp)

Seats / Engines

2 seats · 1 engine

Last airworthiness date

19560323

ADS-B equipped

Yes — Mode-S A146C0

Registrant of record

WOF AERO LTD

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Factual narrative

WHILE CLIMBING THRU APRX 400 TO 500 FT AFTER TAKEOFF, THE PLT MADE A SLIGHT RGT TURN WHICH WAS FLWD BY A LEFT BANK. AFTER MOVING THE CONTROL STICK FOR A LEFT BANK, IT JAMMED TO THE LEFT & WAS RESTRICTED IN FORE & AFT MOVEMENT. THE PLT APPLIED FULL RGT RUDDER & ALTERNATED BTN FULL & PARTIAL PWR. THIS PLACED THE ACFT IN A SKID. SUBSEQUENTLY, IT DSCNDD & STRUCK A 60 TO 70 FT PWR LINE, THEN CAME TO REST IN A FIELD. AN EXAM REVEALED THERE WAS A PLASTIC FUEL SAMPLER & A CLOTH PITOT COVER WITH A METAL CLIP IN THE BELLY OF THE FUSELAGE. MARKINGS WERE FND WHICH VERIFIED THE SAMPLER HAD WEDGED BTN THE CONTROL STICK INTERCONNECT TUBE & THE FUSELAGE STRUCTURE. WHEN THE SAMPLER WAS PLACED IN THAT PSN AFTER THE ACDNT, THE CONTOLS WOULD JAM AS DESCRIBED BY THE PLT. AN EXAM FOR PSBL SOURCES OF FOREIGN OBJECTS REVEALED THERE WERE OPENINGS AT BOTH BOOT COVERS FOR THE CONTROL STICKS. BOTH BOOT COVERS WERE DETERIORATED. ALSO, THERE WAS A 2' CUT-OUT WHERE THE UPPER ELEV CONTROL CABLE EXTENDED UPWARD FM THE FLOORBOARD AT THE REAR BULKHEAD. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1987_BFO87FA048.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.