NTSB CAROL · Event
Event CEN25FA198
Registry · N1846E
FAA Aircraft Registry record.
Make / Model
AERONCA 7AC
Year of manufacture
1946 · 79 years old at event
Engine
CONT MOTOR A&C65 SERIES (65 hp)
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19750902
ADS-B equipped
Yes — Mode-S A152B7
Registrant of record
BLUE NORTHERN SKY FLUTE LLC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Factual narrative
On June 7, 2025, about 1459 central daylight time, an Aeronca 7AC airplane, N1846E, sustained substantial damage when it was involved in an accident near Waterman, Illinois. The pilot was fatally injured, and the passenger was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. According to witness reports, the pilot took his 3-year-old grandson for a ride to drop a homemade parachute made from a 16 ounce water bottle in a plastic grocery bag suspended below a homemade parachute made from black plastic. The parachute was dropped and the pilot reported over the radio that he was coming back around to see where the parachute landed. Witnesses observed the airplane maneuvering just west of the airport property; the right wing dipped, the nose dropped into a sudden dive, and an increase in engine power was heard. The wings leveled but the dive was not arrested before the airplane impacted terrain. The airplane came to rest about 250 ft west of the Hinkley Airport (0C2), Hinkley, Illinois, property in a cultivated field. The top cowl over the engine was at a 37° nose down angle to the ground with the engine at the same attitude. The top portion of the fuselage from the firewall aft was deformed to the left. The left wing was in line with its normal position but with the fuselage deformity the left wing struts laid flat on the ground. The right wing remained attached to the fuselage, but the right wing struts exhibited impact damage, and the wing was angled downward with its wingtip nearly resting on the ground. All three landing gear separated from the airplane and the fuel tank was ejected about 10-15 feet forward of the airplane. The airplane, engine, and propeller were examined at the accident site and no anomalies were found that would have prevented normal operation of the airplane. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2025_CEN25FA198.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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