NTSB CAROL · Event
Event CEN17LA044
Aircraft involved
Probable cause & findings
The pilot's failure to properly position the fuel selector before takeoff, which resulted a total loss of engine power due to fuel starvation.
Factual narrative
On November 23, 2016, about 1115 central standard time, a Cessna 182P airplane, N7392Q, was substantially damaged during a forced landing following a loss of engine power on initial climb after takeoff from runway 36 (4,004 feet by 60 feet, asphalt) at the Bridgeport Municipal Airport (XBP), Bridgeport, Texas. The pilot sustained serious injuries and the passenger sustained minor injuries. The airplane was registered to Skypartners LLC and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91 as a personal flight. Visual meteorological conditions prevailed for the flight, which was operated on an instrument flight rules (IFR) flight plan. The flight had originated shortly before the accident.The pilot reported that they departed Hutchinson Regional Airport (HUT) about 0827. The intended destination was the New Braunfels Regional Airport (BAZ), with a planned fuel stop at XBP. After fueling the airplane at XBP, she obtained an IFR clearance to BAZ. The takeoff was "normal" until about 200 ft above ground level when the engine "suddenly stopped completely." Her efforts to restore engine power were not successful and she executed a forced landing straight ahead. The airplane touched down "hard" in the pasture off the end of the runway and impacted a row of trees before coming to a stop. The passenger reported that the takeoff proceeded "uneventfully" and the engine ran "smoothly." However, shortly after takeoff as the airplane neared the end of the runway, the engine lost power. The airplane landed "very hard" in the grass beyond the end of the runway and struck trees. A witness reported that the airplane first touched down about 1,000 feet beyond the departure end of the runway in the middle of a field. The airplane subsequently bounced, touched down again, and impacted a tree. The propeller separated after the airplane contacted the tree. He responded to the accident site and observed the fuel selector in the Off position at that time. He noted that fuel was pouring from the right-wing fuel tank. The responding Texas Highway Patrol Trooper stated that both the pilot and passenger independently informed him that they believed the fuel selector was in the "wrong" position during takeoff. They had stopped for fuel and did not reset the selector prior to departure. The accident site was located about 500 yards north of the runway 36 departure threshold, according to the Federal Aviation Administration inspector that responded to scene. A postrecovery examination of the airplane was conducted by an FAA inspector, with technical assistance from representatives of the airframe and engine manufacturers. No anomalies consistent with a preimpact failure or malfunction were observed. The pilot reported that the takeoff was "normal" until about 200 ft above ground level, when the engine "suddenly stopped completely." Her efforts to restore engine power were not successful, and she executed a forced landing straight ahead. The airplane touched down "hard" in a pasture off the end of the runway and impacted a row of trees before coming to a stop. A witness that responded to the accident site stated that the fuel selector was in the off position. A responding law enforcement officer stated that both the pilot and passenger independently informed him that they believed the fuel selector was in the "wrong" position during takeoff. A postrecovery examination of the airframe and engine did not reveal any anomalies consistent with a preimpact failure or malfunction; therefore, it is likely that the engine experienced a total loss of engine power due to fuel starvation. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Personnel issues-Action/decision-Action-Forgotten action/omission-Pilot - C
- C Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot - C
- C Aircraft-Aircraft systems-Fuel system-Fuel selector/shutoff valve-Incorrect use/operation - C
- C Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid management - C
- — Personnel issues-Task performance-Use of equip/info-Use of checklist-Pilot
Verbatim from NTSB's published report. Source file
NTSB_2016_CEN17LA044.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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