Skip to content

Atlas / NTSB / DCA85IA019

NTSB CAROL · Event

Event DCA85IA019

1985-04-25 DETROIT, Michigan, United States Minor 1 aircraft Status: Completed

Registry · N9663

FAA Aircraft Registry record.

Make / Model

BEECH G36

Seats / Engines

6 seats · 1 engine

ADS-B equipped

Yes — Mode-S AD7531

Registrant of record

CFL PARTNERS INC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Factual narrative

THE FLT CREWMEMBERS OF THE JUMBO JET WERE PREPARING TO START THE ENGS WHEN FLT ATTENDANTS (F/A'S) IN THE FORWARD CABIN DETECTED A FAINT ODOR PRIOR TO CLOSING DOOR 1L. THE SOURCE COULD NOT BE DETERMINED, SO THE DOOR WAS CLOSED IN PREPARATION FOR A PUSHBACK. SHORTLY THEREAFTER, SMOKE WAS DISCOVERED IN THE VICINITY OF THE OVERHEAD BIN AT ROW 16. THE CAPTAIN WAS NOTIFIED & HE ORDERED THAT 'OCCUPANTS EVACUATE, IF THERE IS A FIRE ONBOARD.' THE JETWAY WAS BROUGHT BACK TO DOOR 1L. THE SMOKE DISSIPATED; THUS, THE F/A'S AT DOORS 1R, 2L & 2R DID NOT OPEN THEIR DOORS. HOWEVER, THE F/A'S AT THE OTHER 6 DOORS WERE UNAWARE OF THE SITUATION & CONTINUED THE EVACUATION. THE RAMPS AT DOORS 3L & 3R DID NOT INFLATE & DOOR 5R JAMMED HALFWAY OPEN. THE RAMP PACKS FOR 3R & 3L WERE IMPROPERLY MOUNTED. THE 5R PACK BOARD WAS MADE FOR A LEFT HAND DOOR & THE LANYARD WAS NOT CONNECTED TO THE BOTTOM PANEL PULLEY. AN EXAM REVEALED A BALLAST FOR AN OVERHEAD FLOURESCENT LIGHT, PN 69-33C, HAD OVERHEATED & MELTED THE PLASTIC CASE. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1985_DCA85IA019.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.