NTSB CAROL · Event
Event ERA17CA186
Aircraft involved
Probable cause & findings
The flight instructor’s and pilot’s mismanagement of the available fuel, which resulted in exhaustion of the fuel in the selected fuel tank and a subsequent total loss of engine power.
Factual narrative
The flight instructor was working with the private pilot on his flight review. Prior to the flight, the pilot checked the fuel and observed that the fuel level in both fuel tanks was below the tabs, and that the right fuel tank had less fuel in it then the left fuel tank. After departing, maneuvering in the local area, the pilot and the flight instructor returned to the airport, landed, then taxied back for another takeoff. After completing two traffic pattern circuits, on the third takeoff the engine stopped producing power at 800 ft. msl, on the upwind leg of the traffic pattern. The private pilot lowered the airplane's nose and the engine started running again. The flight instructor then took over control of the airplane as they started on the right crosswind leg for the runway, and at 900 ft. msl, the engine lost power again. After deciding that the airplane did not have enough altitude, to make the runway, she advised the air traffic control tower that they were going to attempt a landing in a field near the airport. She then checked the mixture, throttle, and ignition, without result, but neither she nor the private pilot, attempted to switch from the right fuel tank to the left fuel tank.During the off-airport landing, the airplane went through an electric fence, spun around about 180 degrees. The nose landing gear sheared off, resulting in substantial damage to the airframe. Examination of the engine revealed no evidence of any preimpact mechanical failures or malfunctions that would have precluded normal operation. Examination and draining of the fuel system, revealed that the fuel strainer bowl, the line from the fuel strainer to the carburetor, and the carburetor float bowl were absent of fuel. The right fuel tank also contained only about 1 pint of fuel, while the left fuel tank contained about 3 gallons of fuel. Review of flight school records revealed that the airplane had flown 4.7 hours since it was last refueled. When asked, the flight instructor advised that she had not observed the private pilot as he performed his preflight inspection, did not know when the airplane had last been refueled, and did not remember asking the private pilot about the fuel quantity before they departed. The flight instructor was working with the private pilot on his flight review. Before the flight, the pilot checked the fuel and observed that the fuel level in both fuel tanks was below the tabs and that the right fuel tank had less fuel in it then the left fuel tank. After departing and maneuvering in the local area, the pilot and the flight instructor returned to the airport, landed, then taxied back for another takeoff. After completing two traffic pattern circuits, on the third takeoff, the engine stopped producing power at 800 ft mean sea level (msl) on the upwind leg of the traffic pattern. The pilot lowered the airplane's nose, and the engine started running again. The flight instructor then took over control of the airplane as they started on the right crosswind leg for the runway, and at 900 ft msl, the engine lost power again. After deciding that the airplane did not have sufficient altitude to reach the runway, the flight instructor advised the air traffic control tower that they were going to attempt a landing in a field near the airport. She then checked the mixture, throttle, and ignition, without results, but neither she nor the private pilot attempted to switch from the right fuel tank to the left fuel tank. During the off-airport landing, the airplane went through an electric fence and spun around about 180°. The nose landing gear sheared off, which resulted in substantial damage to the airframe. Examination of the engine revealed no evidence of any preimpact mechanical failures or malfunctions that would have precluded normal operation. Examination and draining of the fuel system revealed that the fuel strainer bowl, the line from the fuel strainer to the carburetor, and the carburetor float bowl were absent of fuel. The right fuel tank also contained only about 1 pint of fuel, whereas the left fuel tank contained about 3 gallons of fuel. Review of flight school records revealed that the airplane had flown 4.7 hours since it was last refueled. When asked, the flight instructor advised that she had not observed the pilot as he performed his preflight inspection, did not know when the airplane had last been refueled, and did not remember asking the pilot about the fuel quantity before they departed. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid management - C
- C Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot - C
- C Personnel issues-Task performance-Use of equip/info-Use of equip/system-Instructor/check pilot - C
- — Personnel issues-Action/decision-Info processing/decision-Decision making/judgment-Pilot
- — Personnel issues-Action/decision-Info processing/decision-Decision making/judgment-Instructor/check pilot
- — Environmental issues-Physical environment-Object/animal/substance-Tree(s)-Contributed to outcome
Verbatim from NTSB's published report. Source file
NTSB_2017_ERA17CA186.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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