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Atlas / NTSB / LAX94LA178

NTSB CAROL · Event

Event LAX94LA178

1994-04-04 CHINO, California, United States Airport · CNO Minor 1 aircraft Status: Completed

Registry · N1451D

FAA Aircraft Registry record.

Make / Model

NORTH AMERICAN/AERO CLASSICS P-51D

Year of manufacture

1944 · 50 years old at event

Engine

PKRD-ROLL V1650 SERIES (1490 hp)

Seats / Engines

1 seats · 1 engine

Last airworthiness date

19751009

ADS-B equipped

Yes — Mode-S A0B7C2

Registrant of record

TEETERS DAVID

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

the pilot's decision to fly an unairworthy and uncertificated airplane, his failure to perform an adequate preflight, and the improper installation of the oil cooler lines.

Factual narrative

On April 4, 1994, at 1749 hours Pacific daylight time, a North American P-51D, N1451D, was substantially damaged during a forced landing at Chino, California. The forced landing was precipitated by a loss of engine power. Visual meteorological conditions prevailed for the personal cross-country flight and no flight plan was filed. The pilot and passenger received minor injuries. The flight originated at Chino at 1745 hours as a local test flight with a planned continuation to Prescott, Arizona. This was the first flight since completion of a major rebuild and restoration. The pilot planned to circle the airport area several times to check the operation of the aircraft prior to departing for Prescott. Ground witnesses stated that they do not recall seeing the airplane go through normal ground power checks prior to flight. While maneuvering in the airport area, the pilot reported that he experienced an oil mist in the cockpit. The pilot declared an emergency and the Chino Air Traffic Control Tower cleared the aircraft to land on runway 21. The aircraft collided with terrain in a cow pasture about 1/4 mile north of the airport. During the postcrash examination of the engine and the oil system, it was observed that the inlet and outlet oil lines to the oil cooler had been inadvertently crossed. An aluminum beaded oil line with a rubber hose and clamp was found disconnected from the cooler on the inlet side. According to a mechanic familiar with the aircraft and engine types, the crossing of these oil lines will cause a pressure build up and can force the hose to uncouple. Examination of the airplane fuselage revealed a trail of engine oil from the oil cooler aft along the belly to the tail.

PERSONNEL INFORMATION

Review of the Federal Aviation Administration (FAA) airman record and medical files revealed that the pilot's last flight physical of record was dated March 23, 1981. At the time of that examination, he reported a total flight time of 8,000 hours with 200 in the last 6 months.

AIRCRAFT INFORMATION

According to the airframe logbook, the last documented aircraft maintenance was performed on April 12, 1987, at a total airframe time of 1,751.3 hours. According to an engine logbook, the engine installed at the time of the accident had been overhauled on May 3, 1983, and had accrued 456.3 hours of operation. The last documented annual inspection was dated April 12, 1987. The airplane was being rebuilt at Chino after a previous accident. The work had been in progress for several years. No inspection, repair, or overhaul data was recovered regarding the restoration or rebuilding of the airplane. The pilot departed with the intention of circling the airport several times to check the aircraft prior to departing on a cross-country to Prescott, Arizona. The airplane was undergoing a major rebuilding and restoration after a previous accident and had not flown for several years. Postcrash examination revealed that two oil cooler lines had been inadvertently crossed. One of the oil cooler lines failed as a result of the incorrect line installation and the engine oil was pumped overboard. The engine subsequently sustained a catastrophic internal failure. The last logbook entry and documented annual inspection for the airplane was dated 1987. The pilot's last flight physical was dated 1981. Ground witnesses stated that the pilot did not go through the normal preflight ground power checks prior to flight. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1994_LAX94LA178.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗