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Atlas / NTSB / LAX96LA066

NTSB CAROL · Event

Event LAX96LA066

1995-11-29 CHINO, California, United States Airport · CNO None 1 aircraft Status: Completed

Registry · N5114N

FAA Aircraft Registry record.

Make / Model

BOEING B75N1

Year of manufacture

1943 · 52 years old at event

Engine

CONT MOTOR W670 SERIES (250 hp)

Seats / Engines

2 seats · 1 engine

Last airworthiness date

19871210

ADS-B equipped

Yes — Mode-S A66817

Registrant of record

SETH MAARTEN A

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

the pilot's failure to see and avoid light poles. A poorly planned approach was a factor.

Factual narrative

On November 29, 1995, about 1315 hours Pacific standard time, a Boeing B75-N1, N5114N, collided with a light pole while executing a low approach north of runway 26 at Chino Airport, Chino, California. The pilot was conducting a local visual flight rules personal flight and he landed the airplane on runway 26 without further incident. The airplane, registered to and operated by a private individual, sustained substantial damage. The certificated private pilot, the sole occupant, was not injured. Visual meteorological conditions prevailed. The flight originated at Chino Airport about 1300 hours. A Federal Aviation Administration (FAA) operations inspector from the Riverside [California] Flight Standards District Office reported this accident to the National Transportation Safety Board on December 7, 1995. He said that a filming company asked the accident pilot and another pilot to execute a low approach over the airport so that they could film their airplanes in the background. The local controller granted the pilot's request to execute a low approach over the airport from the east to the west. During the low approach, the left wing of the accident aircraft struck the top of an aluminum light pole. The pilot reported in a letter to the FAA that he was asked by an unknown person to slow to 70 knots indicated airspeed while on final approach for the low pass. He said that since he was offset to the north his approach was much steeper than normal. He said that he allowed the airspeed to drop off too much and he leveled off at a lower altitude than anticipated. When he added power to stabilize the airplane, the left wing struck the pole that he did not see. After contacting the pole, the airplane remained stable and he landed on runway 26 without further incident after reentering the traffic pattern. The pilot had been asked by a film crew to execute a low pass over the runway. The local controller granted the pilot's request to execute a low pass offset to the north of the runway. When on final approach, the pilot allowed the airspeed to decrease and made a steep approach to the runway. The pilot failed to see the light poles north of the runway. The airplane's left wing contacted the light poles. The pilot did not lose control of the airplane and reentered the traffic pattern landing without further incident. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1995_LAX96LA066.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.