NTSB CAROL · Event
Event LAX98IA061
Aircraft involved
Probable cause & findings
An emergency evacuation due to fumes from a failed hydraulic line that entered into the cabin.
Factual narrative
On December 19, 1997, at 1815 hours Pacific standard time, the crew of an Alaska Airlines MD-80, N932AS, operating as Flight 536 from Palm Springs, California, to San Francisco, California, under 14 CFR Part 121, ordered an emergency evacuation after experiencing noxious fumes entering the aircraft. Visual meteorological conditions existed at the time. There was no damage to the aircraft and no injuries to the 5 crewmembers or to the 69 passengers. According to the operator, the aircraft was taxiing to the gate after landing when fumes and mist began to enter the cabin through the air conditioning ducts. Although first noted as thin, the vapors quickly filled the cabin, reducing visibility, and causing respiratory distress along with burning eyes to crew and passengers. The crew elected to stop the aircraft on the taxiway near the intersection of "A" and "H" taxiways. The captain ordered an immediate evacuation over the aircraft's public address system. The crew estimated the evacuation was accomplished within 90 seconds. After the evacuation, the flight attendants commented on having to divest passengers of carry-on baggage during the evacuation. A concern was that the baggage taken from the passengers could block the path to the exit(s). All flight attendants commented on how useful they found their flashlights to be. All retrieved their flashlights before proceeding to the exits and found them to be invaluable during the evacuation, as well as on the ground. Subsequent investigation revealed the source of the vapors as a failed hydraulic return line from the left-hand engine thrust reverser. Leaking fluid from the line was ingested into the aircraft's APU that had been started by the flight crew after landing in accordance with normal procedures. The captain ordered an emergency evacuation after noxious fumes and mist entered the aircraft during the taxi to the gate after landing. Examination of the aircraft found the source of the vapors as a failed hydraulic return line from the left-hand engine thrust reverser. Leaking fluid from the line was ingested into the aircraft's APU which had been started in accordance with normal procedures. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_1997_LAX98IA061.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
Beyond the agency record
Search this event elsewhere.
Pre-filled searches into the sources where news + community discussion of aviation events lives. External sources are reported, not agency. Treat them as signal that something happened, not as fact about what happened.
Entity-clustered aviation events in the press — last 24 hr + 30-day archive.
Official agency record + docket.
Investigative docket: factual reports, photos, transcripts.
Long-running aviation incident database (Flight Safety Foundation).
Community NTSB synthesis blog — often has photos and witness reports.
Gold-standard aviation incident blog.
Aviation industry news search.
GA pilot forum — informed but rumor-prone.
GA pilot subreddit search.
Tail-number page — flight history (free tier limited).
AOPA Air Safety Institute search.
Mainstream press coverage. Recent events only.
Privacy-preserving news search.
External links open in a new tab. We don't ingest their content; we deep-link search queries.