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Atlas / NTSB / WPR14LA123

NTSB CAROL · Event

Event WPR14LA123

2014-02-25 Corona, California, United States Airport · KAJO None 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The loss of engine power during initial climb for reasons that could not be determined because a postaccident examination of the engine did not reveal any anomalies that would have precluded normal operation.

Factual narrative

On February 25, 2014, about 1230 Pacific standard time, a Lake LA-4-200 airplane, N1040L, sustained substantial damage during an emergency descent and landing at the Corona Airport (KAJO), Corona, California. The airplane was owned and being operated by the pilot as a visual flight rules (VFR), personal local flight, under the provisions of 14 Code of Federal Regulations Part 91. The solo airline transport pilot was not injured. Visual meteorological conditions prevailed at the time of the accident, and no flight plan was filed for the local area flight. During a telephone conversation with the National Transportation Safety Board investigator-in-charge on February 25, the pilot said he had not flown the airplane for about 3 weeks. He stated that his intent was to fly the airplane in the airport traffic pattern, and perform several full stop landings. He said prior to takeoff during the run-up, the engine ran rough on the right magneto. After he leaned the mixture, the problem resolved itself, and he proceeded to complete the pre-takeoff checklist. After the first takeoff and landing, he proceeded to take off again, climbed to about 800 feet above ground level, and the engine lost power. The pilot reported that he turned back toward the airport, but when he determined he would not make the runway he steered toward an open grassy area on the airport, and prepared the airplane for landing. During landing, he side-loaded the left main landing gear, which collapsed, resulting in substantial damage to the fuselage. The pilot said prior to the flight, he had not had any mechanical problems with the airplane. He stated that he did not fuel the airplane prior to the flight, and believed that the tank had been one-quarter full. On March 19, at the direction of the NTSB IIC, and under the supervision of an FAA air safety inspector, the accident airplane's engine was test run. The airplane was first inspected and found in suitable condition for an engine run. No fuel was added. The airplane has a single central main fuel tank. The tank is conical in shape with the taper at the bottom. The tank configuration results in no unusable fuel, and places the engine pickup and fuel sump drain at the lowest point in the tank. The engine was started per the airplane's checklist, and run with the electric auxiliary fuel pump in both the on and off position. No mechanical anomalies were found during the engine run. The pilot reported that he intended to fly the airplane in the airport traffic pattern and perform several full-stop landings. During the engine run-up before the first takeoff, the engine ran roughly on the right magneto. The pilot leaned the fuel mixture, which resolved the problem. He then completed the pretakeoff checklist, and, subsequently, he took off in the airplane, completed the pattern, and made a full-stop landing. During the second takeoff, the pilot climbed the airplane to about 800 feet above ground level where the engine lost power. After turning the airplane back toward the airport, the pilot determined that the airplane would not reach the runway, so he maneuvered the airplane toward an open grassy area on the airport. During the landing, he side-loaded the left main landing gear, which subsequently collapsed. A postaccident test run of the airplane's engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. The reason for the loss of engine power could not be determined. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Malfunction

Verbatim from NTSB's published report. Source file NTSB_2014_WPR14LA123.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.