NTSB CAROL · Event
Event DFW07CA097
Aircraft involved
Probable cause & findings
The pilot's failure to compensate for existing wind conditions while landing. A contributing factor was the prevailing crosswind.
Factual narrative
The 160-hour private pilot lost control of the single-engine airplane while performing takeoff and landings on Runway 17. Runway 17 was reported to be 6,110-feet long, by 75-feet wide. The asphalt runway was reported to be dry and in good condition at the time of the mishap. The pilot, who reported having accumulated 128-hours in the same make and model aircraft, reported that he planned to stay in the traffic pattern to practice takeoffs and landings. The winds at the time of the mishap were reported from 080 degrees at 13 knots, gusting to 16 knots. During the third landing on Runway 17, the pilot was reported to have landed long, approximately 2,500-feet from the landing threshold, rolled for a short distance, and abruptly veer to the left, departing the runway on a heading of 120-degrees. The nose landing gear collapsed, the engine firewall and engine mounts sustained structural damage. The pilot confirmed that aircraft controls and engine performance were normal. The pilot and his passenger were able to egress the airplane unassisted and were not injured. The 160-hour private pilot lost control of the single-engine airplane while performing takeoff and landings on Runway 17. Runway 17 was reported to be 6,110-feet long, by 75-feet wide. The asphalt runway was reported to be dry and in good condition at the time of the mishap. The pilot, who reported having accumulated 128-hours in the same make and model aircraft, reported that he planned to stay in the traffic pattern to practice takeoffs and landings. The winds at the time of the mishap were reported from 080 degrees at 13 knots, gusting to 16 knots. During the third landing on Runway 17, the pilot was reported to have landed long, approximately 2,500-feet from the landing threshold, rolled for a short distance, and abruptly veer to the left, departing the runway on a heading of 120-degrees. The nose landing gear collapsed, the engine firewall and engine mounts sustained structural damage. The pilot confirmed that aircraft controls and engine performance were normal. The pilot and his passenger were able to egress the airplane unassisted and were not injured. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2007_DFW07CA097.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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