Skip to content

Atlas / NTSB / CHI08CA048

NTSB CAROL · Event

Event CHI08CA048

2007-12-11 Elyria, Ohio, United States Airport · LPR None 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The pilot's momentary loss of control after takeoff, which resulted in an in-flight collision with a tree. A contributing factor was the presence of the tree.

Factual narrative

The pilot reported that he departed on an instrument flight rules flight plan into a low overcast cloud ceiling. He commented that he lost visual contact with the ground immediately upon liftoff. During the initial climb, the airplane momentarily entered a nose-down attitude. He subsequently corrected the nose down attitude. However, as the airplane began to climb again the right wing impacted a tree. This occurred approximately 1 mile from the airport and within 1 minute of takeoff. After the in-flight collision, he had "full function" of the airplane and elected to continue the planned 31-minute flight to the intended destination. He added that there were no anomalies related to flight control or engine operation during the flight. A post accident inspection revealed impact damage to the leading edge of the right wing, right engine nacelle, and right propeller spinner. In addition, the inspection revealed a 3-inch crack in the aft wing spar at the right main landing gear wheel well. The pilot reported that he departed on an instrument flight rules flight plan into a low overcast cloud ceiling. He commented that he lost visual contact with the ground immediately upon liftoff. During the initial climb, the airplane momentarily entered a nose-down attitude. He subsequently corrected the nose down attitude. However, as the airplane began to climb again the right wing impacted a tree. This occurred approximately 1 mile from the airport and within 1 minute of takeoff. After the in-flight collision, he had "full function" of the airplane and elected to continue the planned 31-minute flight to the intended destination. He added that there were no anomalies related to flight control or engine operation during the flight. A post accident inspection revealed impact damage to the leading edge of the right wing, right engine nacelle, and right propeller spinner. In addition, the inspection revealed a 3-inch crack in the aft wing spar at the right main landing gear wheel well. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2007_CHI08CA048.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (loss of control). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗