NTSB CAROL · Event
Event LAX04LA094
Registry · N305BD
FAA Aircraft Registry record.
Make / Model
CESSNA 305A
Year of manufacture
1950 · 54 years old at event
Seats / Engines
2 seats · 1 engine
Last airworthiness date
19791114
ADS-B equipped
Yes — Mode-S A33202
Registrant of record
QUALITAIR LLC TRUSTEE
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The failure of a tail wheel steering component (spring), which resulted in a loss of directional control and a ground loop during the landing roll. A contributing factor was the soft terrain adjacent to the runway.
Factual narrative
On January 14, 2004, about 1526 mountain standard time, a Cessna 305A, N305BD, ground looped during landing rollout at the Casa Grande Municipal Airport, Casa Grande, Arizona. The airplane was owned/operated by the pilot, and it was substantially damaged. Neither the airline transport certificated pilot nor the passenger was injured. The flight was performed under the provisions of 14 CFR Part 91. Visual meteorological conditions prevailed, and no flight plan had been filed. The flight originated about 2 hours earlier from Blythe, California. The pilot verbally reported to the National Transportation Safety Board investigator that he had recently purchased the airplane, and he was in the process of flying it to his North Carolina home. The pilot indicated that the wind was nearly calm when he landed on runway 05. However, upon touchdown the airplane bounced. During his recovery, he lost directional control when the airplane began swerving. In the pilot's completed "Aircraft Accident Report," he described the sequence of events leading to the accident in the following manner: I made contact with the runway in a three-point configuration, but I was not in a full stall. I ballooned into the air about a foot coming back to contact the runway in a full stall three-point landing, but with the nose of the aircraft about 10 to 15 degrees off to the right. It felt as if the right wing stalled a fraction of a second before the left wing, causing it to swing. This may not be what happened to the wing. While I was trying to straighten the aircraft with the left rudder and a short burst of power, the right wheel got off into the sand causing a ground loop to the right. The pilot subsequently indicated to the Safety Board investigator that the accident touchdown had not been perfect, but it was definitely not hard. After touching down and observing the airplane begin to swerve, he applied full left rudder in an effort at regaining directional control. However, his effort was unsuccessful. When the pilot completed the Safety Board's "Aircraft Accident Report" he indicated that no mechanical malfunction was related to the accident. However, following the airplane's subsequent examination the pilot verbally reported to the Safety Board investigator that one of the airplane's tail wheel rudder control springs was broken. The pilot also reported that he has over 4,000 hours of accident and incident free piloting experience in tail wheel airplanes, with over 400 hours in a Cessna 305A. He reported a total pilot time in excess of 28,000 hours. The airplane was manufactured in the mid-1950s. The pilot lost directional control during landing. During the landing rollout, the airplane veered off the side of the runway, entered a sandy area adjacent to the runway and ground looped. At the time, the wind was nearly calm. The pilot had planned to touch down in a three-point configuration, but the airplane was not fully stalled. Upon touchdown it bounced about 1 foot into the air, and touched down again. Neither touchdown was hard. During the landing roll the pilot applied pressure to the rudder pedals in an effort at maintaining directional control. However, despite application of engine power and rudder pressure, his efforts were unsuccessful, and directional control was lost. During the subsequent airframe examination, one of the airplane's tail wheel rudder control springs was found broken. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2004_LAX04LA094.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2026 · Conference Paper
Computational Analysis of Steady State Aerodynamics of Transonic Truss-Braced Wing Configuration in Deep Stall
This study presents a computational investigation of steady state aerodynamics of the Subsonic Ultra-Green Aircraft Research (SUGAR) Transonic Truss-Braced Wing (TTBW) configuration over a wide range …
- arXiv 2023 · arXiv preprint
Automating Bird Diverter Installation through Multi-Aerial Robots and Signal Temporal Logic Specifications
This paper tackles the task assignment and trajectory generation problem for bird diverter installation using a fleet of multi-rotors.
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- arXiv 2023 · arXiv preprint
Polycrystallinity enhances stress build-up around ice
Damage caused by freezing wet, porous materials is a widespread problem, but is hard to predict or control. Here, we show that polycrystallinity makes a great difference to the stress build-up process…
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- Embry-Riddle Scholarly Commons 2021 · Journal article (JAAER)
Analysis on the Negative Emotional, Physiological, and Cognitive Responses Elicited from of the Activation of a Stall Alarm
Failing to identify an aerodynamic stall can lead to the inability of an aircraft to sustain flight. To warn pilots of an impending or fully-developed stall, many aircraft have safety devices installe…
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