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Atlas / NTSB / ANC07LA071

NTSB CAROL · Event

Event ANC07LA071

2007-07-31 Talkeetna, Alaska, United States None 1 aircraft Status: Completed

Registry · N70020

FAA Aircraft Registry record.

Make / Model

AIRBUS A319-115

Year of manufacture

2014

TCDS

A28NM · AIRBUS SAS

Engine

CFM INTL CFM56-5B7

Seats / Engines

147 seats · 2 engines

Last airworthiness date

20140910

ADS-B equipped

Yes — Mode-S A95745

Registrant of record

UMB BANK NA TRUSTEE

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The loss of engine power during cruise flight due to an improperly repaired airbox.

Factual narrative

On July 31, 2007, about 1530 Alaska daylight time, a float-equipped Cessna 185E airplane, N70020, sustained substantial damage when it collided with trees during an emergency descent/landing, following a loss of engine power during cruise flight, about 6 miles southeast of Talkeetna, Alaska. The airplane was being operated by the pilot as a visual flight rules (VFR) cross-country flight in conjunction with his fish guiding service under Title 14, CFR Part 91, when the accident occurred. The commercial certificated pilot and sole passenger were not injured. Visual meteorological conditions prevailed, and no flight plan was filed. The flight departed Stephan Lake, Alaska, about 1500. During a telephone conversation with the National Transportation Safety Board (NTSB) investigator-in-charge (IIC) on August 1, the pilot said he was flying from Stephan Lake to Lake Hood, Alaska, cruising at 2,500 feet msl, and was about 20 minutes into the flight when the airplane's engine went to idle rpm, and the airplane started to descend. The pilot said he pushed the throttle forward, and he thought the engine rpm increased slightly, then returned to idle. He said he had turned the airplane toward a lake, but it descended too rapidly, and he landed in trees short of the lake. The airplane sustained extensive damage to the wings and fuselage. The pilot said that the airplane had sat on the water at Stephan Lake for two days prior to the flight, and that he drained the fuel tank sumps prior to takeoff. He said the airplane's fuel tanks were half-full on departure, which was more than enough fuel for the trip. The pilot said that there were no known mechanical problems with the airplane prior to the flight. After being recovered, the airplane was examined by a certificated aircraft mechanic. The mechanic discovered that the support shaft for the throttle and mixture bell cranks was missing. The air induction box assembly was examined by the IIC, and it was discovered that the air box had been repaired with incorrectly substituted parts. The air box (PN 1650012-1) installed in the accident airplane was the correct air box, however, a weld repair had been performed around the shaft support bushings on both sides of the box. The correct solid shaft bushings had been replaced with earlier generation roller bearings. The inappropriate installation did not allow for the support shaft to be properly pinned in place, and did not allow for the redundant safety of the correct installation, which would preclude the shaft from migrating out of the air box if either shaft end spacer were missing. An examination of the airplane's maintenance log books did not reveal any entries pertaining to the air box repair. The float-equipped airplane was being operated by the commercial pilot as a VFR cross-country flight in conjunction with his guiding service. The pilot said that he departed one lake en route to another, and about 20 minutes into the flight, the engine went to idle rpm. He said he pushed the throttle forward, and turned the airplane toward a lake, but the airplane descended into trees short of the lake. The airplane sustained extensive damage to the wings and fuselage. The pilot said that there were no known mechanical problems with the airplane prior to the flight. The airplane was examined, and it was found that the support shaft for the throttle and mixture bell cranks was missing, which disconnected the throttle control and allowed the engine to go to idle. The air induction box assembly was examined by the NTSB investigator, and it was discovered that the air box had been repaired with incorrectly substituted parts. The air box (PN 1650012-1) was the correct air box; however, a weld repair had been performed around the shaft support bushings on both sides of the box. The correct solid shaft bushings had been replaced with earlier generation roller bearings. The inappropriate installation did not allow for the support shaft to be properly pinned in place, and did not allow for the redundant safety of the correct installation. The correct parts installation would preclude the support shaft from migrating out of the air box if either shaft end spacer were missing. An examination of the airplane's maintenance log books did not reveal any entries pertaining to the air box repair. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2007_ANC07LA071.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗