NTSB CAROL · Event
Event ANC18LA038
Aircraft involved
Probable cause & findings
An inadequate fuel supply to the engine, which resulted in a total loss of engine power and subsequent impact with terrain.
Factual narrative
On May 23, 2018, about 1630 Alaska daylight time, a Belite Pipper, experimental amateur built airplane, N3748, sustained substantial damage during a forced landing, following a total loss of engine power at Lake Hood Seaplane Base (PLHD), Anchorage, Alaska. The airplane was registered to a private individual and operated by the pilot as a 14 Code of Federal Regulations (CFR) Part 91 visual flight rules flight when the accident occurred. The private pilot sustained minor injuries. Visual meteorological conditions prevailed, and no flight plan had been filed. The flight departed PLHD for a local flight in the airport traffic pattern. According to the pilot, the accident flight was the first flight since maintenance was performed on the airplane's fuel system. The pilot stated that he departed Runway 32 and entered a right downwind to remain in the traffic pattern. While on final approach to Runway 32, he elected to execute a go-around. After advancing the throttle, when about 150 ft above ground level (AGL), all engine power was lost. He said the engine quit like there was no fuel. He did not see or hear anything that would be consistent with a mechanical failure. During the forced landing, the pilot attempted to land back on the runway, but touched down between the runway end lights, bounced, and became airborne again. With no remaining runway surface available, the airplane descended into a fence and came to rest inverted in marshy terrain about 375 ft from the departure end of Runway 32. The airplane sustained substantial damage to the fuselage and both wings. A post-accident examination of the Rotax 912 UL2 engine was performed by the NTSB investigator-in-charge along with another NTSB investigator. After removing the rocker box covers, all rocker arms exhibited discoloration consistent with high heat exposure. When the number 4 cylinder was removed, the valve was discovered fractured and a witness mark was present consistent with piston contact. The engine had been altered from its original state by the addition of an Edge Performance Big Bore Kit. The kit, considered a high displacement cylinder/piston kit, was to increase performance and horsepower of the engine. As a result of the modification, the fuel requirements increased over that of a stock 912 UL2 engine. As installed, the kit replaced the crankshaft, camshaft, engine gaskets, cylinders and pistons. The fuel supply system remained the same and no modifications were made to the carburetors. The pilot stated in a phone conversation that he had been discussing with the kit manufacturer a problem with fuel flow to the engine, which is why he was performing maintenance on it the day before and day of the accident. He said he had replaced all fuel lines and fittings with larger fuel lines but made no changes to the carburetors. During subsequent ground tests, fuel flow at the carburetors was measured between 1.8 – 2.0 psi. Prior to the above-mentioned maintenance, after allowing the engine to warm up, when he would apply full power, the engine would quit and the carburetor bowls would be empty. The pilot stated that since the engine continued to run after changing the fuel lines, the "ground tests seemed good with the exception of the fuel pump pressure." The pilot stated that he was conducting a postmaintenance flight in the experimental amateur-built airplane in the traffic pattern. While landing, he applied full throttle to go around, but when the airplane was about 150 ft above ground level, the engine lost total power. During the forced landing, the airplane landed long, bounced, descended into a fence, and came to rest inverted, which resulted in substantial damage to the fuselage and both wings. The engine had been altered from its original state by the addition of an after-market, high-displacement cylinder/piston kit to increase performance and horsepower of the engine. The kit, as installed, replaced the crankshaft, camshaft, engine gaskets, cylinders, and pistons. The pilot stated that he had been discussing with the kit manufacturer a problem with fuel flow to the engine and, thus, altered the fuel supply system with larger fuel lines. No modifications were made to the carburetors. Because the carburetors were not altered, it is likely that the engine was not receiving enough fuel for full power operation, which resulted in a total loss of engine power during the go-around attempt. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Fluids/misc hardware-Fluids-Fuel-Not specified - C
- C Aircraft-Aircraft systems-Fuel system-Fuel distribution-Design - C
Verbatim from NTSB's published report. Source file
NTSB_2018_ANC18LA038.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, go-around, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- Embry-Riddle Scholarly Commons 2023 · Conference paper
The Value of Strong Partnerships to Build a Successful Aviation Maintenance Career Pathway Program for Transitioning Military Service Members
The aerospace industry is competing with other industries for a qualified workforce, and many of those competing industries are investing heavily in creating workforce development pipelines.
- Embry-Riddle Scholarly Commons 2026 · Journal article (IJAAA)
From Reactive to Predictive: A hybrid Trust-Mediated Adoption Framework for Data-Driven Maintenance in Distributed-Authority Aviation Environments
Modern aviation maintenance operates within increasingly data-intensive technological environments, yet the operational integration of predictive maintenance into routine decision-making remains incon…
- NASA NTRS 2026 · Conference Paper
Computational Analysis of Steady State Aerodynamics of Transonic Truss-Braced Wing Configuration in Deep Stall
This study presents a computational investigation of steady state aerodynamics of the Subsonic Ultra-Green Aircraft Research (SUGAR) Transonic Truss-Braced Wing (TTBW) configuration over a wide range …
- NASA NTRS 2025 · Conference Paper
A Training Study to Improve Monitoring During A Go-Around
As part of an FAA program to improve go-around (GA) safety, we were asked to determine if we could improve the performance of the Pilot Monitoring (PM) during a GA maneuver.
- Semantic Scholar 2025 · Article (Applied Sciences)
Decision-Making Framework for Aviation Safety in Predictive Maintenance Strategies
The implementation of predictive maintenance (PM) in aviation presents unique challenges due to strict safety requirements, complex operational environments, and regulatory constraints.
- Flight Safety Foundation 2024 · FSF / AeroSafety World
Go-Around Safety Forum Findings
Foundation Go-Around Safety Forum technical findings — examines why pilots fail to execute go-arounds when criteria are met (stabilized approach gate not met, energy state out of envelope, traffic con…
Browse the full corpus — academia portal ↗