NTSB CAROL · Event
Event ANC24LA005
Registry · N691YW
FAA Aircraft Registry record.
Make / Model
DIAMOND AIRCRAFT DA 40
Year of manufacture
2006 · 17 years old at event
Engine
LYCOMING IO-360-M1A+ (180 hp)
Seats / Engines
4 seats · 1 engine
Last airworthiness date
20061122
ADS-B equipped
Yes — Mode-S A930A8
Registrant of record
GEORGE'S AVIATION SERVICES INC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
A partial loss of engine power due to lose baffling from the muffler, which resulted in an obstruction of the exhaust system.
Factual narrative
On December 04, 2023, about 1250 Hawaii-Aleutian standard time, a Diamond DA-40 airplane, N691YW, sustained substantial damage when it was involved in an accident in Kapolei, Hawaii. The pilot sustained minor injuries, and the designated pilot examiner sustained serious injuries. The airplane was operated by the pilot as a Title 14 Code of Federal Regulations Part 91 flight test. The pilot reported that an engine run-up inspection was completed without any issues of concern before departure. They departed from Danial K Inouye International Airport (PHNL) Honolulu, Hawaii, about 1235. After departure they leveled off at 1,500 ft mean sea level and proceeded to the practice area to conduct an evaluation for an airplane instrument rating. The pilot configured the airplane for the first maneuver. When he moved the throttle control lever forward, they heard a “pop” sound come from the engine, followed by a rumbling noise and an airplane vibration. The pilot pulled the throttle back to its original position in an attempt to stop the rumbling and vibrations and turned the airplane back toward runway 11 at Kalaeloa Airport (PHJR), Kapolei, Hawaii, for an emergency landing. They scanned the ignition, control levers, fuel selector, and multi-function display. The pilot confirmed that the mixture control lever was full forward, the propeller control lever was full forward, and the throttle control lever was about 3/4 full forward. The ignition was positioned on "BOTH", the fuel selector knob was positioned directly over the right tank, and the multi-function display showed no discrepancies in engine instrument readings that would indicate a need for immediate corrective action. The airplane started a descent without any manual pitch adjustments. They increased the throttle lever to the full forward position, but this did not provide any additional thrust from the engine. They declared an emergency; the designated pilot examiner took the flight controls, and they began to look for a suitable area for a forced landing. They performed a forced landing to a flat area of land that was covered with dirt. After initial touchdown, the airplane continued to roll straight down the dirt path until it impacted a dirt hill, resulting in substantial damage to the fuselage and both wings. A postaccident examination conducted by a Federal Aviation Administration inspector and a certified airframe and powerplant mechanic revealed no internal failure of the engine. The fuel injection servo control was in the full throttle position and the mixture control was in the full rich position; neither cable could be moved in the cockpit due to impact damage. The fuel injection servo was removed for inspection, and it revealed that the throttle/butterfly did not move and was in the full-throttle position. The valve covers and lower sparkplugs were removed; no anomalies were noted. No obstructions were observed in the fuel system. The air filter was removed with no obstruction observed. Internal baffling in the exhaust muffler had broken loose and had blocked about 3/4 of the opening. The last 100-hour inspection was completed on November 15, 2023, with the engine total time of 2,290.5 hours While enroute the pilot moved the throttle control lever forward and heard a “pop” sound come from the engine, followed by a rumbling noise and an airplane vibration. The pilot pulled the throttle back to its original position in an attempt to stop the rumbling and vibrations and turned the airplane back toward the runway for an emergency landing. Engine power was not restored, and the airplane began to lose altitude, so the pilot performed a forced landing, which resulted in substantial damage to the fuselage and both wings. Postaccident examination revealed that baffling from the exhaust muffler had broken loose, blocking about 3/4 of the opening. The blocked exhaust reduced the volumetric efficiency of the engine cylinders, resulting in the partial loss of engine power. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- — Aircraft-Aircraft power plant-Engine exhaust-Collector/nozzle-Damaged/degraded
Verbatim from NTSB's published report. Source file
NTSB_2023_ANC24LA005.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
Beyond the agency record
Search this event elsewhere.
Pre-filled searches into the sources where news + community discussion of aviation events lives. External sources are reported, not agency. Treat them as signal that something happened, not as fact about what happened.
Entity-clustered aviation events in the press — last 24 hr + 30-day archive.
Official agency record + docket.
Investigative docket: factual reports, photos, transcripts.
Long-running aviation incident database (Flight Safety Foundation).
Community NTSB synthesis blog — often has photos and witness reports.
Gold-standard aviation incident blog.
Aviation industry news search.
GA pilot forum — informed but rumor-prone.
GA pilot subreddit search.
Tail-number page — flight history (free tier limited).
AOPA Air Safety Institute search.
Mainstream press coverage. Recent events only.
Privacy-preserving news search.
External links open in a new tab. We don't ingest their content; we deep-link search queries.