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Atlas / NTSB / ATL00IA035

NTSB CAROL · Event

Event ATL00IA035

2000-03-05 KEY LARGO, Florida, United States Airport · X09 None 1 aircraft Status: Completed

Registry · N314QS

FAA Aircraft Registry record.

Make / Model

EMBRAER S A EMB-505

Year of manufacture

2013

Engine

P&W CANADA PW535E

Seats / Engines

9 seats · 2 engines

Last airworthiness date

20130820

ADS-B equipped

Yes — Mode-S A3571C

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The malfunction of the nose gear locking mechanism for undetermined reason.

Factual narrative

On March 5, 2000, at 1200 eastern standard time, a Cessna CE-560, N314QS, nose gear collapsed during a normal landing at the Ocean Reef Club Airport in Key Largo, Florida, The on demand air taxi positioning flight was operated by Executive Jet Incorporated under the provisions of Title 14 CFR Part 91 with a flight plan filed. Visual weather conditions prevailed at the time of the incident. The airplane sustained minor damage, and the two air transport pilots were not injured. The positioning flight departed Palm Beach, Florida, at approximately 1130. According to the pilot, the before landing check, which included the lowering of the landing gear, was completed several miles on short final. The pilot recalled that the landing gear indicator lights were green or indicated that the landing gear was down and locked. After the airplane landed, the pilot deployed the thrust reverses. At approximately the same time, the nose gear retracted into the wheel well. The airplane slid down runway 04, and came to rest 2000 feet from the end of the runway. The preliminary examination of the airplane disclosed that the nose gear up-down-lock actuator assembly experienced a mechanical failure. During the subsequent examination of the assembly no mechanical problem was detected during functional testing. All functional pressures and other operational parameters tested within the normal certificated limits. The pilot completed the before landing check, which included the lowering of the landing gear, several miles on short final. The pilot recalled that the landing gear indicator lights were green, or landing gear down and locked. After the airplane landed, the pilot deployed the thrust reverses. At approximately the same time, the nose gear retracted into the wheel well. The airplane slid down runway 04, and came to rest 2000 feet from the end of the runway. The initial examination of the airplane disclosed that the nose gear up-down-lock actuator experienced a mechanical failure. During the subsequent examination of the assembly, no mechanical problem was detected during functional testing. All functional pressures and other operational parameters tested within the normal certificated limits. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2000_ATL00IA035.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type. Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗