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Atlas / NTSB / ATL02LA164

NTSB CAROL · Event

Event ATL02LA164

2002-08-30 Panacea, Florida, United States Airport · 2J0 None 1 aircraft Status: Completed

Registry · N9097F

FAA Aircraft Registry record.

Make / Model

BARKER JOHN HOME BUILT

Year of manufacture

2002 · 0 years old at event

Engine

LYCOMING 0-235 SERIES (115 hp)

Seats / Engines

2 seats · 1 engine

Last airworthiness date

20020114

ADS-B equipped

Yes — Mode-S AC93EE

Registrant of record

FOWLER DAVID J

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The builders inadequate weld on the nose gear u-shaped bracket, that resulted in the nose wheel strut failure, and subsequent nose over during an attempted landing.

Factual narrative

On August 30, 2002, at 1430 eastern daylight time, a John Barker experimental airplane, N9097F, registered to and operated by the pilot, nosed over inverted during landing at the Wakulla County airstrip in Panacea, Florida. The personal flight was operated under the provisions of Title 14 CFR Part 91 with no flight plan filed. The private pilot reported no injuries, and the airplane sustained substantial damage. The flight originated at Perry Foley Airport in Perry, Florida, about 1330. The pilot stated he flew a normal approach to runway 18 at 70 knots. He stated the airplane touched down on the main landing gear at 60 knots, and when the nose wheel touched down, the airplane bounced three to four feet into the air. He stated the airplane touched down on the main landing gear again, and when the nose settled on the runway, the airplane immediately flipped inverted. The pilot stated the turf runway has a rough, bumpy surface. Initial examination of the airplane revealed the nose wheel was separated, the vertical stabilizer and rudder sustained crush damage, and the propeller was damaged. The pilot stated the nose wheel was found about 60 feet from the fuselage near visible tracks in the turf where the main landing wheels initially touched down. The pilot stated the u-shaped aluminum bracket bolted to the nose wheel strut was found broken at the weld. Further examination by two welding experts revealed that the weld was "insufficient" on the shear points of the u-shaped aluminum bracket, and the weld had not completely penetrated the metal. The pilot flew a normal approach to a rough, bumpy turf runway. The airplane touched down on the main landing gear at 60 knots, and when the nose wheel touched down, the airplane bounced three to four feet into the air. The airplane touched down on the main landing again, and when the nose settled on the runway, the airplane immediately flipped inverted. Examination of the airplane revealed the nose wheel was separated and the vertical stabilizer and rudder sustained crush damage. The pilot stated the nose wheel was found about 60 feet from the fuselage. The pilot stated the u-shaped aluminum bracket bolted to the nose wheel strut was found broken at the weld. Further examination by two welding experts revealed that the weld was "insufficient" on the shear points of the u-shaped aluminum bracket, and the weld had not completely penetrated the metal. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2002_ATL02LA164.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type. Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗