Skip to content

Atlas / NTSB / CEN16CA359

NTSB CAROL · Event

Event CEN16CA359

2016-08-26 Wichita Falls, Texas, United States Airport · CWC None 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The incorrect maintenance of the airplane's ventilation system which resulted in an obstruction of the elevator control system.

Factual narrative

The pilot reported that, during a maintenance test flight, when the airplane reached rotation speed on takeoff, he applied elevator control to rotate. The elevator control could not be moved sufficiently aft for rotation and liftoff, and the pilot aborted the takeoff. During the aborted takeoff, the airplane travelled off the departure end of the runway and came to a stop on an airport access road. The airplane's left main landing gear collapsed and the left wing was bent during the accident. The pilot reported that he had performed a control system check prior to the flight and that the controls functioned normally during that check. Examination of the airplane revealed that the elevator control operated normally after the accident, but further examination revealed that a plastic elbow fitting for the windshield defroster duct was loose and could be rotated into a position that obstructed full motion of the control yoke. Examination of the elbow revealed that it was not an approved part and appeared to be the type of plastic elbow found in home supply stores. The recent maintenance performed was not in the area where the plastic elbow was located. The pilot reported that, during a maintenance test flight, when the airplane reached rotation speed on takeoff, he applied elevator control to rotate. The elevator control could not be moved sufficiently aft for rotation and liftoff, and the pilot aborted the takeoff. During the aborted takeoff, the airplane travelled off the departure end of the runway and came to a stop on an airport access road. The airplane's left main landing gear collapsed and the left wing was bent during the accident. The pilot reported that he had performed a control system check prior to the flight and that the controls functioned normally during that check. Examination of the airplane revealed that the elevator control operated normally after the accident, but further examination revealed that a plastic elbow fitting for the windshield defroster duct was loose and could be rotated into a position that obstructed full motion of the control yoke. Examination of the elbow revealed that it was not an approved part and appeared to be the type of plastic elbow found in home supply stores. The recent maintenance performed was not in the area where the plastic elbow was located. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • C Aircraft-Aircraft systems-Flight control system-Elevator control system-Inoperative - C
  • C Aircraft-Aircraft systems-Air conditioning system-Air distribution system-Incorrect service/maintenance - C

Verbatim from NTSB's published report. Source file NTSB_2016_CEN16CA359.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗