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Atlas / NTSB / CEN21LA176

NTSB CAROL · Event

Event CEN21LA176

2021-04-03 Pearland, Texas, United States Airport · T79 None 1 aircraft Status: Completed

Registry · N5240C

FAA Aircraft Registry record.

Make / Model

BEECH B35

Engine

CONT MOTOR E185 SERIES (205 hp)

Seats / Engines

4 seats · 1 engine

Last airworthiness date

19560106

ADS-B equipped

Yes — Mode-S A69A25

Registrant of record

HARDY PETE

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The partial loss of engine power due to a crack in the No. 1 cylinder for unknown reasons.

Factual narrative

On April 3, 2021, about 0730 central daylight time, a Beech B35 airplane, N5240C, was substantially damaged when it was involved in an accident near Pearland, Texas. The pilot and three passengers were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that he conducted a thorough preflight and runup with no anomalies noted. The pilot performed a short-field takeoff from a grass runway and lowered the nose of the airplane to gain airspeed while in ground effect. The pilot reported that there was a difference in the engine sound, and the engine did not have the power it normally had. The engine speed was at “2,100 rpm and dropping.” The pilot was unable to climb the airplane above the powerlines in his flight path and he decided to fly under them. While maneuvering the airplane to land in a field, the right wing struck a tree, separating the wing from the fuselage. The pilot landed the airplane on its belly, and it skidded across the grass before it came to rest. The airplane sustained substantial damage to both wings and the fuselage. The pilot stated that he purchased the airplane in October 2020 and that the airplane had undergone extensive maintenance to troubleshoot excessive engine rpm issues. The pilot noted that the airplane flew uneventfully for the first time on the day before the accident. A mechanic had examined the airplane just before the accident flight and found no anomalies. An examination of the engine after the accident revealed a crack between the No. 1 cylinder head and bore. According to the maintenance records, on October 1, 2016, all 6 cylinders were removed and replaced with serviceable cylinders and new piston rings. The cylinders had 324.3 hours since overhaul at the time of installation. It is estimated the cylinders accumulated about 60 hours between the time of installation and the accident. The pilot reported that immediately after takeoff he noted a difference in the sound of the engine and that the engine speed started to decrease. The airplane was unable to climb above obstacles along the flight path, and the pilot elected to conduct a forced landing. During the forced landing the right wing struck a tree, and the airplane came to rest in a field. The airplane sustained substantial damage to both wings and the fuselage. A postaccident engine examination revealed a crack between the No. 1cylinder head and bore. The engine likely lost power due to this crack; however, the origin of the crack was not identified. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft power plant-Power plant-(general)-Malfunction
  • Not determined-Not determined-(general)-(general)-Unknown/Not determined

Verbatim from NTSB's published report. Source file NTSB_2021_CEN21LA176.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗