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Atlas / NTSB / CEN23LA351

NTSB CAROL · Event

Event CEN23LA351

2023-08-06 Holliday, Texas, United States None 1 aircraft Status: Completed

Registry · N2005J

FAA Aircraft Registry record.

Make / Model

TAYLORCRAFT AVIATION CORP. F21

Engine

LYCOMING 0-235 SERIES (115 hp)

Seats / Engines

2 seats · 1 engine

Last airworthiness date

19810821

ADS-B equipped

Yes — Mode-S A19513

Registrant of record

GRAY SHANE CHARLES

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

A loss of engine power for reasons that could not be determined, which resulted in impact with terrain.

Factual narrative

On August 6, 2023, about 2000 central daylight time, a Taylorcraft Aviation Corporation F21 airplane, N2005J, sustained substantial damage when it was involved in an accident near Holliday, Texas. The pilot and the passenger were not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot departed from a private grass airstrip near Holliday, Texas, for the local flight. While established on the approach to the airstrip, the pilot felt the airplane needed additional engine power to clear trees and reach the runway. The pilot started to apply the throttle, but the airplane continued to sink. The pilot then applied full engine power to execute a go-around but realized that the engine was not producing power. The pilot observed that the engine did not stop operating but was not responsive to his throttle inputs. The pilot did not hear any abnormal noises from the engine, noting “[t]here were no coughing or sputtering noises to my recollection.” The left wing impacted a tree about 30 ft short of the airstrip and the airplane came to rest upright on a grass field. The pilot shut down the airplane and the two occupants egressed without further incident. The airplane sustained substantial damage to the fuselage and both wings. Postaccident examination of the airframe revealed flight control continuity. The two wing fuel tanks were found intact. The wing tanks fed into a header tank, which appeared to be intact and full of fuel. Engine control continuity was established from the cockpit. Examination of the engine found no mechanical anomalies. The pilot reported that he was not using carburetor heat on the approach. He stated that he was on a mile final and was carrying some power. Comparison of the weather conditions at the time of the accident to the Federal Aviation Administration’s Special Airworthiness Information Bulletin CE-09-35 indicated that the conditions were not conducive to carburetor icing. The pilot reported that the throttle cable might have been the potential cause for the lack of response from the engine, as there was a previous problem with the throttle cable “slipping.” The throttle cable was adjusted by a mechanic on March 18, 2023, about four and a half months before the accident, and the pilot reported that the maintenance work corrected the slippage issue. During the postaccident examination, the throttle was found installed, intact, and there were no signs of any missing hardware. When the pilot purchased the airplane in September 2022, the most recent annual inspection had been completed in November 2011. A mechanic performed an annual inspection on the airframe and the engine on October 28, 2022. The pilot was landing the airplane at a private runway when he added additional engine power to clear trees and reach the runway. The pilot started to apply the throttle, but the airplane continued to sink. The pilot then applied full engine power to execute a go-around, but realized the engine was not producing power. The pilot observed that the engine did not stop operating but was not responsive to his throttle inputs. The pilot did not hear any abnormal noises from the engine, noting “[t]here were no coughing or sputtering noises to my recollection.” The left wing impacted a tree about 30 ft short of the runway and the airplane came to rest upright on a grass field. The pilot shut down the airplane and the two occupants egressed without further incident. The airplane sustained substantial damage to the fuselage and both wings. Postaccident examination of the airframe and engine found no mechanical anomalies. The pilot reported that the throttle cable might have been the potential cause for the lack of response from the engine, as there was a previous problem with the throttle cable “slipping.” During the postaccident examination, the throttle was found installed, intact, and there were no signs of any missing hardware. Although the pilot reported that he was not using carburetor heat on the approach, he indicated that on the final approach he was “carrying some power.” Additionally, the weather conditions at the time of the accident were not conducive to carburetor icing. Accordingly, the reason for the loss of engine power and the engine’s unresponsiveness to the pilot’s throttle inputs could not be determined. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Not determined-Not determined-(general)-(general)-Unknown/Not determined
  • Aircraft-Aircraft power plant-Engine (reciprocating)-(general)-Unknown/Not determined

Verbatim from NTSB's published report. Source file NTSB_2023_CEN23LA351.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (icing, stall, go-around, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗