Skip to content

Atlas / NTSB / CEN24LA065

NTSB CAROL · Event

Event CEN24LA065

2023-12-17 Burnet, Texas, United States Airport · BMQ Serious 1 aircraft Status: Completed

Registry · N70SL

FAA Aircraft Registry record.

Make / Model

BEECH B36TC

Year of manufacture

1986 · 37 years old at event

Engine

CONT MOTOR TSIO-520 SER (300 hp)

Seats / Engines

6 seats · 1 engine

Last airworthiness date

19861118

ADS-B equipped

Yes — Mode-S A953D0

Registrant of record

MCLEOD SAMMY DALE JR

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The loss of engine power due an overly rich mixture from an improper adjustment of the fuel pump, which resulted in a forced landing and impact with a car and terrain.

Factual narrative

On December 17, 2023, about 1414 central standard time, a Beech B36TC, N70SL, was destroyed when it was involved in an accident near Burnet, Texas. The pilot and passenger received serious injuries. The airplane was operated under Title 14 Code of Federal Regulations as a Part 91 personal flight. The pilot stated the preflight, engine start, engine runup, and takeoff roll were normal. While climbing through 200 to 300 ft agl, the engine began to surge and lose power. The airplane was unable to climb, and the pilot was unsuccessful using emergency procedures at regaining engine power. The pilot said he could not see an area suitable to land on except for a road. During the landing, the airplane’s right wing struck a car and exploded into flames. The airplane landed in a field and was destroyed by impact forces and postcrash fire. A witness stated that he saw the airplane intermittently emitting black smoke from the exhaust as it climbed out slowly after takeoff. A video of the takeoff showed dark smoke emitting from the airplane’s exhaust area. A second witness saw the airplane fly southbound at an estimated altitude of 100 to 150 ft agl and was having difficulty gaining altitude. The airplane’s landing gear was retracted, the wing flaps were retracted, and the propeller was turning. The airplane lost altitude and descended behind a hill. The engine-driven fuel pump assembly was removed for testing at Continental Aerospace Technologies, Mobile, Alabama, under the supervision of the NTSB Investigator-in-Charge. The fuel pump assembly was placed on a test bench and during testing at an input speed of 2,700 rpm, the fuel flow was 38.42 gallons per hour and the maximum limit for the test was 34.9 gallons per hour. There was no test fluid leakage from the fuel pump assembly during the test. The fuel pump assembly was removed from the test bench and disassembled to determine the length of its internal aneroid. The fuel pump assembly’s aneroid adjustment screw was extended outward 0.4480 inch. The internal aneroid was not elongated and was of comparable length to the aneroid of a new production fuel pump assembly, which indicated a normal condition. According to Continental Aerospace Technologies, the greater the outward extension of the aneroid adjustment screw, the greater the output of fuel flow from the fuel pump assembly. A review of the engine maintenance logbooks showed that the fuel pump was overhauled in June 2004, and that the engine was overhauled April 14, 2022. There were no other references to work or adjustments done on the fuel pump. The Federal Aviation Administration Aviation Maintenance Technician Handbook–Powerplant (2023), Chapter 10, Engine Maintenance & Operation, Engine Troubleshooting, Figure 10-52, lists symptoms of a rich mixture to include black exhaust smoke and sluggish engine operation. The pilot stated the preflight, engine start, engine runup, and takeoff roll were normal. While climbing through 200 to 300 ft above ground level (agl) after takeoff, the engine began to surge and lose power. Black smoke was seen coming from the airplane’s exhaust during the takeoff and climb. The airplane was unable to climb, and the pilot was unsuccessful using emergency procedures at regaining engine power. The pilot said that the only area suitable for landing that he saw was a road. During the landing, the airplane’s right wing struck a car, and the airplane exploded into flames. The airplane came to rest in a field and was destroyed by impact forces and postcrash fire. Postaccident examination and testing of the engine-driven fuel pump revealed that it was adjusted for a fuel flow that exceeded the maximum limitation for the pump. Symptoms of a rich mixture to include black exhaust smoke and sluggish engine operation, were witnessed during the airplane’s takeoff and climb. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft systems-Fuel system-(general)-Not specified
  • Aircraft-Aircraft systems-Fuel system-Fuel pumps-Incorrect service/maintenance

Verbatim from NTSB's published report. Source file NTSB_2023_CEN24LA065.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗