NTSB CAROL · Event
Event CHI03LA163
Registry · N2238E
FAA Aircraft Registry record.
Make / Model
CESSNA 172N
Seats / Engines
4 seats · 1 engine
ADS-B equipped
Yes — Mode-S A1EF9B
Registrant of record
IRON STREET AVIATION LLC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The pilot's failure to attain the proper touchdown point, and his failure to maintain directional control. Contributing factors were the pilot's lack of experience, and the runway sign.
Factual narrative
On June 14, 2003, at 0901 central daylight time, a Cessna 172N, N2238E, operated by Anoka Flight Training as a rental/instructional flight, sustained substantial damage when it veered off runway 36 (4,855 feet by 100 feet, asphalt) and struck an airport sign during landing roll at Anoka County-Blaine Airport (ANE), Blaine, Minnesota. Visual meteorological conditions prevailed at the time of the accident. The 14 CFR Part 91 student solo flight was not operating on a flight plan. The pilot reported no injuries. The local flight originated from ANE at 0700. According to the pilot, he was attempting to land on runway 36. The pilot reported that as the airplane touched down it was slightly left of the runway centerline, and the airplane bounced twice. The pilot stated that as he regained control of the airplane it was leaving the runway at which time it struck a runway sign, collapsed the nose gear, and the propeller struck the ground. The weather conditions at ANE at 0855 were: wind 060 degrees at 6 knots; visibility 10 statute miles; sky conditions clear. The student pilot accumulated a total flight time 30 hours all of which were in the make and model of the accident airplane. The pilot reported no mechanical malfunctions or failures. The airplane was substantially damaged when it veered off runway 36, struck a runway sign, and collapsed the nose landing gear. The student pilot reported that when he landed the airplane he was left of the runway centerline. When he regained control the airplane was leaving the runway. The weather conditions at the airport were: wind 060 degrees at 6 knots; visibility 10 statute miles; sky conditions clear. No mechanical anamolies with the airplane were noted. The student pilot accumulated a total flight time 30 hours all of which were in the make and model of the accident airplane. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2003_CHI03LA163.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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