NTSB CAROL · Event
Event CHI03LA184
Registry · N8413D
FAA Aircraft Registry record.
Make / Model
BELL 47G-5A
TCDS
2H3 · SCOTT'S-BELL 47 INC
Engine
LYCOMING VO-435 SERIES (260 hp)
Seats / Engines
3 seats · 1 engine
Last airworthiness date
19860521
ADS-B equipped
Yes — Mode-S AB8655
Registrant of record
EXPERIMENTAL AIRCRAFT ASSOCIATION INC
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The failure of the ignition switch leading to an engine power loss in cruise flight and the subsequent high flare during autorotation. Factors contributing to the accident were the pilot's misjudgment of the landing flare and the unsuitable terrain encountered by the pilot on landing.
Factual narrative
On June 27, 2003, at 2100 eastern daylight time, a Bell 47G-5A helicopter, N8413D, operated by Adventure Helicopters Inc., sustained substantial damage during an autorotation following an in flight loss of engine power near Sandusky, Michigan. Visual meteorological conditions prevailed at the time of the accident. The airline transport pilot and his two passengers reported no injuries. The 14 CFR Part 91 business flight was not operating on a flight plan. The local flight departed a private helipad near Sandusky, Michigan, about 2100. The pilot reported the engine failed at approximately 400 feet above ground level. The pilot noted he performed a 180-degree autorotation to the southwest. The pilot stated he thought "it was evident that [the helicopter was] going to land in a large drainage ditch. I elected to flare sooner than I wanted to avoid the ditch." The pilot reported the helicopter subsequently landed hard in a bean field. A FAA airworthiness inspector conducted an on-scene inspection of the helicopter. The inspection showed engine and control surface continuity and all cylinders exhibited compression. Both fuel tanks contained fuel and the spark plugs and exhaust tubes were clean. The two magnetos worked independently. The inspection revealed that the ignition switch had an internal fault. The helicopter sustained substantial damage when it landed hard during an autorotation following an in-flight loss of engine power. The pilot reported the engine failed at approximately 400 feet above ground level while in cruise flight. The pilot noted he performed an autorotation but flared early to avoid a drainage ditch. The pilot stated the helicopter landed hard in a field. An inspection of the helicopter showed engine and flight control continuity. The spark plugs and exhaust tubes were clean and the fuel tanks contained fuel. The magnetos worked when tested independently of the ignition system. The inspection revealed that the ignition switch had an internal fault causing it to ground out the ignition system. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2003_CHI03LA184.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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