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Atlas / NTSB / CHI96LA044

NTSB CAROL · Event

Event CHI96LA044

1995-12-01 NEWTON, Kansas, United States Airport · EWK Minor 1 aircraft Status: Completed

Registry · N95SF

FAA Aircraft Registry record.

Make / Model

SMITH WILLIAM S SMITH COZY MARK IV

Seats / Engines

4 seats · 1 engine

ADS-B equipped

Yes — Mode-S AD33E4

Registrant of record

SMITH WILLIAM S

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

a loss of engine power for undetermined reasons. A factor related to the accident was the presence of traffic requiring the pilot to perform an evasive maneuver.

Factual narrative

On December 1, 1995, at 1300 central standard time (cst), a Herring Dana Sport Fan, N95SF, owned and operated by a private pilot, was substantially damaged during a forced landing, shortly after takeoff from runway 17 at Newton City Airport, Kansas. The pilot reported minor injuries. Visual meteorological conditions prevailed at the time of the accident. The personal 14 CFR Part 91 flight was not operating on a flight plan. From the pilot's written statement, the airplane made a normal takeoff, at approximately 300 feet the engine lost total power. After an unsuccessful restart, the pilot attempted to land on a paved road. The pilot stated, "...glide was extended to avoid traffic. As a result, the airspeed was too low and descent rate could not be arrested ... ." The airplane came to rest in a ravine alongside the road. Post accident examination of the airplane by the Federal Aviation Administration Principal Maintenance Inspector (PMI), revealed low compression on one out of the two cylinders. The pilot/owner believes the problem might have been an ignition problem. During takeoff, the airplane experienced a total loss of engine power. The pilot maneuvered the airplane to avoid traffic. As a result, the airspeed became too low and the descent rate could not be stopped. The airplane slid off the paved roadway into a ravine. Postaccident examination revealed the engine had low compression in one of the two cylinders. The pilot stated he thought the loss of power resulted from an ignition problem. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1995_CHI96LA044.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗