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Atlas / NTSB / DEN00LA001

NTSB CAROL · Event

Event DEN00LA001

1999-10-01 GALLUP, New Mexico, United States Airport · GUP Serious 1 aircraft Status: Completed

Registry · N716JB

FAA Aircraft Registry record.

Make / Model

GRAY JIM ROBERT EXEC

Engine

ROTORWAY RW-145 SERIES (145 hp)

Seats / Engines

2 seats · 1 engine

Last airworthiness date

19980615

ADS-B equipped

Yes — Mode-S A99321

Registrant of record

GRAY JIM R

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The pilot inadvertently allowing main rotor rpm to decay while avoiding obstacles during an emergency autorotation following a loss of power for reasons undetermined. Factors were houses and powerlines.

Factual narrative

On October 1, 1999, approximately 0645 mountain daylight time, a Gray Rotorway Executive homebuilt helicopter, N716JB, registered to and operated by the pilot, was destroyed when it collided with terrain during descent at Gallup, New Mexico. The solo student pilot was seriously injured. Visual meteorological conditions prevailed, and no flight plan had been filed for the instructional flight being conducted under Title 14 CFR Part 91. The flight originated at Gallup, New Mexico, approximately 0630. In his accident report, the pilot said he intended on remaining in the traffic pattern to practice touch and go landings. He had purposely planned the early morning flight because the "wind is usually calm and density altitude is lowest, giving the helicopter best performance capabilities." The flight was uneventful until the helicopter reached the point where the pilot would turn from downwind to base leg, and he noticed the "rotor rpm was low (95%)." He turned the helicopter towards the runway and "lowered collective [to] stabilize rotor rpm." At this point, "the engine failed." He "lowered collective [control] all the way down, [pushed] the cyclic [control] forward, and began autorotation." The helicopter descended toward houses, so he "extended [the descent path] by pulling collective." Rotor rpm fell to 80%. The pilot headed towards a small open field but as he descended to 100 feet agl (above ground level), he noticed powerlines ahead. He did a "second extension," and power dropped to 60%. Approximately 30 feet agl, he pulled the nose up and added full up collective to arrest the descent. The helicopter struck the ground tail first, then rolled over on its left side. In December 1999, the engine was functionally tested at the facilities of Rotorway in Chandler, Arizona. Despite impact damage to the crankshaft, the engine operated normally. The pilot remained in the traffic pattern to practice touch and go landings. At approximately the point where the helicopter would turn onto the base leg, rotor rpm began to decay (95%). The pilot turned towards the runway and began autorotation. During the descent, the pilot managed to avoid houses and powerlines. The helicopter struck the ground tail first, then rolled over on its left side. The engine was later functionally tested and, despite impact damage to the crankshaft, operated normally. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1999_DEN00LA001.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.