NTSB CAROL · Event
Event ERA15LA237
Aircraft involved
Probable cause & findings
The pilot’s failure to properly set the stabilator trim prior to takeoff, which resulted in an exceedance of the airplane’s critical angle of attack and an aerodynamic stall during takeoff.
Factual narrative
On June 14, 2015, about 0930 eastern daylight time, a Piper PA-28-140, N43078, impacted trees and terrain shortly after takeoff from Hampton Airfield (7B3), Hampton, New Hampshire. The private pilot and one passenger received serious injuries. The airplane was substantially damaged by impact forces and a postcrash fire. Visual meteorological conditions prevailed and no flight plan was filed for the planned flight to Biddeford Airport (B19), Biddeford, Maine. The airplane was owned and operated by the private pilot under the provisions of Title 14 Code of Federal Regulations Part 91 as a personal flight.According to the pilot, on the morning of the accident he had fueled the airplane at B19, and performed a "full run-up and normal takeoff" for the flight to 7B3. The takeoff, all systems, and flight characteristics appeared normal. After landing at 7B3, he taxied to the ramp and shut the airplane down. He did not refuel at 7B3, and a short time later he and his passenger embarked and taxied to runway 02, where he performed another engine run-up, with no anomalies noted. He indicated that the takeoff, and all systems including the airspeed, appeared normal. He said that the airplane lifted off at 65 knots, but it would not climb. He asked the passenger to read the emergency checklist, and verified that the mixture was rich, the throttle was full, the fuel selector was on the fullest tank, the fuel pump was on, and the carburetor heat was off. He attempted to keep the airplane level; however, he raised the nose at the last minute as they approached a tree line. The airplane cleared the initial tree line; however, subsequently descended into the wooded area. According to a witness, as the airplane lifted off from the runway, it appeared to have a "high angle of attack," and it looked as though it was "mushing through the air" after takeoff. During the initial climb the pitch attitude decreased briefly, and then increased before the airplane reached a tree line. After clearing the trees, the nose lowered and the airplane disappeared out of sight. The witness further stated that he did not hear a loss of engine power at any time. Another witness stated that when the airplane lifted off the ground, its "nose was too vertical." The witness thought the airplane would not climb above the trees in the nose-up position; however, it cleared the tree tops and was "nearly vertical" when it began to lose altitude. Review of airport surveillance video also revealed that the airplane lifted off and remained in a nose-up attitude. Examination of the wreckage, at the scene, by a Federal Aviation Administration (FAA) inspector revealed that the airplane impacted a wooded area about 2,000 feet from the departure end of the runway and slightly right of the extended runway centerline. The fuselage came to rest upright in a nose down attitude with the engine and nose section embedded in soil. Both wings were separated from the fuselage. A postaccident examination of the airplane and engine was conducted by an FAA inspector and representative from the engine manufacturer. One propeller blade exhibited chordwise scratching and leading-edge gouging. When the engine crankshaft was rotated by hand, continuity was confirmed on all cylinders, valves, and accessory gears. Thumb compression and suction was verified on each cylinder. The spark plugs were removed and examined; each displayed little or no wear and were light gray/black/oily in color. The carburetor bowl was removed and was found to be free of debris. Control cable continuity was established from each aileron though fractures, consistent with tensile overload, to the cockpit area. The stabilator and rudder were removed during salvage recovery efforts, and the flight control cables were cut by recovery personnel. However, cable continuity was confirmed from the cockpit area to the rudder and stabilator. Examination of the stabilator trim indicator in the cockpit revealed that the trim was in the full nose up position. Examination of the stabilator trim jackscrew revealed 16 exposed threads, which equated to a full nose-up position. Review of a takeoff checklist from a make and model pilot operating manual revealed "Trim tab – set." The private pilot reported that the airplane lifted off normally but would not climb. The airplane cleared trees at the end of the runway before descending and impacting a wooded area. Two witnesses reported and airport surveillance video confirmed that the airplane lifted off in an extreme nose-up attitude and remained in that attitude as it descended below trees at the end of the runway. Examination of the wreckage did not reveal any preimpact mechanical malfunctions. During the examination, the stabilator trim was found in the full nose-up position. The pre-takeoff checklist for the airplane included instructions to properly set the stabilator trim prior to takeoff. It is likely that the stabilator trim position resulted in the airplane's extreme nose-up attitude, which led to an exceedance of the airplane's critical angle of attack during the initial climb and an aerodynamic stall. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Aircraft systems-Flight control system-Elevator control system-Incorrect use/operation - C
- C Personnel issues-Action/decision-Action-Incorrect action selection-Pilot - C
- C Aircraft-Aircraft oper/perf/capability-Performance/control parameters-Angle of attack-Capability exceeded - C
- C Personnel issues-Task performance-Use of equip/info-Aircraft control-Pilot - C
Verbatim from NTSB's published report. Source file
NTSB_2015_ERA15LA237.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- NASA NTRS 2026 · Conference Paper
Computational Analysis of Steady State Aerodynamics of Transonic Truss-Braced Wing Configuration in Deep Stall
This study presents a computational investigation of steady state aerodynamics of the Subsonic Ultra-Green Aircraft Research (SUGAR) Transonic Truss-Braced Wing (TTBW) configuration over a wide range …
- arXiv 2023 · arXiv preprint
Automating Bird Diverter Installation through Multi-Aerial Robots and Signal Temporal Logic Specifications
This paper tackles the task assignment and trajectory generation problem for bird diverter installation using a fleet of multi-rotors.
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- arXiv 2023 · arXiv preprint
Polycrystallinity enhances stress build-up around ice
Damage caused by freezing wet, porous materials is a widespread problem, but is hard to predict or control. Here, we show that polycrystallinity makes a great difference to the stress build-up process…
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- Embry-Riddle Scholarly Commons 2021 · Journal article (JAAER)
Analysis on the Negative Emotional, Physiological, and Cognitive Responses Elicited from of the Activation of a Stall Alarm
Failing to identify an aerodynamic stall can lead to the inability of an aircraft to sustain flight. To warn pilots of an impending or fully-developed stall, many aircraft have safety devices installe…
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