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Atlas / NTSB / ERA24LA139

NTSB CAROL · Event

Event ERA24LA139

2024-03-12 Front Royal, Virginia, United States Airport · FRR None 1 aircraft Status: Completed

Registry · N59MK

FAA Aircraft Registry record.

Make / Model

BEECH K35

Year of manufacture

1959 · 65 years old at event

Engine

CONT MOTOR I0-470 SERIES (260 hp)

Seats / Engines

5 seats · 1 engine

Last airworthiness date

19590811

ADS-B equipped

Yes — Mode-S A79C2B

Registrant of record

TFF INC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

A total loss of engine power due to fuel starvation as a result of the pilot’s mismanagement of the airplane’s fuel supply.

Factual narrative

On March 12, 2024, about 1902 eastern standard time, a Beech K35, N59MK, was substantially damaged when it was involved in an accident near Front Royal, Virginia. The pilot was not injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 aerial observation flight. The pilot departed on an aerial survey flight from Shannon Airport (EZF), Fredericksburg, Virginia, at 1301. The pilot reported that, during the flight, he attempted to adjust the propeller control with no response. The pilot slowed the airplane as he approached the survey area and the propeller became responsive, so he elected to continue with the survey. During the survey, he noted that the No. 3 cylinder exhaust gas temperature (EGT) value was low, which was abnormal. He continued the flight to see if the EGT would return to more normal indications, but it did not, and he chose to discontinue the survey and land at the destination airport. He began to climb the airplane and attempted to switch fuel tanks from the right main tank to the left main tank, but several minutes later, the engine began to stumble. He double-checked the fuel selector position and noted that it was on an auxiliary fuel tank, so he switched it to the left main fuel tank, and continued to climb to 6,300 ft. About 10 minutes later, the engine lost total power. He turned toward the nearest airport and attempted to restore power, but was unsuccessful. Realizing that the airplane would not reach the airport, the pilot performed a forced landing to a field, during which the airplane traveled through a tree line and the outboard portions of both wings separated from the airplane. The pilot stated that he departed with the airplane fueled to its full capacity (99 gallons), and that the airplane was equipped with six fuel tanks. The pilot also commented that the engine was recently overhauled and had accrued fewer than 100 hours since the field overhaul was completed. The airplane was equipped with two bladder-type main fuel tanks, one per wing, each with a capacity of 25 gallons, of which 3 gallons were unusable. It was also equipped with two bladder-type auxiliary fuel tanks, each with a 20-gallon capacity, of which 1 gallon was unusable. The airplane was also equipped with fiberglass wingtip fuel tanks. While the wreckage was being recovered from the accident site, personnel from the recovery company removed about 5 gallons of fuel from the right wing fuel tanks and less than 1 gallon from the left wing fuel tanks. The wreckage was subsequently taken to an aircraft salvage facility for additional examination. The main and auxiliary fuel tanks did not display indications that they had been breached during the accident sequence. The wingtip tanks remained attached to the wings but were both ruptured. The main fuel tanks were cut adjacent to wing skin cuts made by recovery personnel to facilitate transportation. Portions of the wing fuel vent plumbing were also cut into sections adjacent to the recovery cuts made to the wings. The wing vent plumbing for each main and bladder tank was found to be free from blockage. The right wing siphon-break plumbing was partly obstructed by dirt near the wing port. The wingtip tank vent plumbing was free from obstructions. The fuel supply lines from each auxiliary fuel tank to the fuel selector were cut adjacent to wing recovery cuts. The fuel supply plumbing was examined, and found to be free from obstructions, by passing air through both the main wing and auxiliary bladder tank plumbing, the fuel selector, and out the fuel strainer outlet. The wingtip tank plumbing was examined and found to be free from obstructions. The airplane’s battery was connected, and the auxiliary fuel pump operated normally. The fuel transfer pumps and solenoid valves were connected to a 12-volt battery and also operated normally. The fuel strainer and fuel strainer bowl were clean. The propeller blades were cut midspan to facilitate a test run of the engine. Automotive gasoline was supplied at the fuel pump inlet from an external source. The fuel pump return was re-routed to the external source. The engine started and the throttle was advanced until the engine rpm reached 2,500. The airplane’s throttle, mixture, and propeller controls were operated with no discrepancies noted. The propeller lever controlled propeller rpm when inputs were applied. The engine test run was conducted for 5 minutes before concluding. A test of the oil transfer collar was performed. Using a differential pressure gauge, 80 psi was applied to the governor oil pressure port. The oil pressure port maintained 42 psi when 80 psi was applied. The propeller governor remained attached to the front of the engine and was undamaged. Control continuity from the governor to the cockpit was established. The propeller governor was removed before the engine test run and the gasket screen was unobstructed. The propeller governor pumped oil when the drive was rotated by hand and was reinstalled to facilitate the engine test run. Following the test run, the propeller governor was sent for bench testing. There were no physical anomalies noted prior to testing and the governor was flushed prior to testing to mitigate any potential contamination from entering the test equipment. The unit was mounted to the test bench and run to reach the proper operating temperature. Once at temperature, the unit passed all of the requirements described per the original manufacturer’s manual requirements. A J.P. Instruments EDM-900 was recovered from the airplane, and data were successfully downloaded from the unit following the engine test-run. Parameters from the accident flight, the postaccident engine test run, and a previous flight were recovered and evaluated. Review of the parameters from the accident flight showed that about 20 minutes prior to the end of the flight, the engine manifold pressure was about 22 inHg, while the engine fuel flow consistently indicated 15 gallons per hour (gph) with a fuel pressure of 15 psi. At 1847:20, the fuel pressure and fuel flow both simultaneously decreased to 0. As the fuel flow and pressure dropped, at 1847:30 the engine rpm increased from 2,600 to about 3,300 rpm before reducing to 2,000 rpm. Concurrently, all six CHTs and EGTs uniformly began to drop to 0. The engine’s manifold pressure also began increasing as the airplane descended. The pilot was conducting an extended duration aerial survey flight. He reported that he had experienced anomalies with the propeller controls and the No. 3 cylinder exhaust gas temperature (EGT) during the flight. After about 5 and ½ hours of flying, he became uncomfortable with the EGT values and chose to suspend the survey and land. He began to climb the airplane while enroute to the destination. During the climb, he attempted to switch the fuel selector from the right main to the left main fuel tank, and several minutes later, the engine began to stumble. He double-checked the fuel selector, noted that it was on an auxiliary tank, then moved it to the left main tank position. He reported that shortly thereafter the engine lost total power. He was unable to reach the destination airport and performed a forced landing to a field, during which the airplane was substantially damaged. The airplane was equipped with two bladder-type main fuel tanks, one per wing, each with a capacity of 25 gallons of which 3 gallons were unusable; and two bladder-type auxiliary fuel tanks, each with a 20-gallon capacity of which 1 gallon was unusable. The airplane was also equipped with fiberglass wingtip tanks. The pilot reported that he departed on the accident flight with all of the fuel tanks filled to their capacity. The main and auxiliary fuel tanks were not breached during the accident sequence, while the wingtip tanks remained attached to the wings but were both ruptured. Personnel who recovered the airplane from the accident site collected about 5 gallons of fuel from the right wing fuel tanks and less than 1 gallon of fuel from the left wing fuel tanks. A subsequent airframe inspection, engine test run, test of the oil transfer collar, and a propeller governor bench test were conducted, and all revealed no evidence of preimpact mechanical malfunctions or failures that would have resulted in a total loss of engine power. Examination of data from the airplane’s engine data monitor revealed that shortly before the engine lost power, the fuel flow and pressure values suddenly decreased to 0, after which the cylinder head temperature (CHT) and EGT also began decreasing. The data were consistent with an interruption of fuel flow to the engine, resulting in a total loss of engine power. In summary, the data which suggest the loss of engine power was preceded by an interruption of fuel flow, the successful posaccident test run of the engine, the lack of any mechanical anomalies found during the poaccident examinations and test runs of the engine and its subcomponents, combined with the limited amount of fuel recovered from the airplane after the accident, were all indicative that the loss of engine power was most likely the result of fuel starvation. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Personnel issues-Task performance-Planning/preparation-Fuel planning-Pilot
  • Aircraft-Fluids/misc hardware-Fluids-Fuel-Fluid management

Verbatim from NTSB's published report. Source file NTSB_2024_ERA24LA139.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, fuel starvation). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗