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Atlas / NTSB / ERA24LA307

NTSB CAROL · Event

Event ERA24LA307

2024-07-01 Greenville, North Carolina, United States Airport · PGV None 1 aircraft Status: Completed

Registry · N9308Q

FAA Aircraft Registry record.

Make / Model

BEECH 95-B55 (T42A)

Year of manufacture

1971 · 53 years old at event

Engine

CONT MOTOR I0-470 SERIES (260 hp)

Seats / Engines

6 seats · 2 engines

Last airworthiness date

19711202

ADS-B equipped

Yes — Mode-S ACE928

Registrant of record

MT ZEPHYR ENTERPRISES LLC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

A landing with the nose gear retracted as a result of an intermittent landing gear relay.

Factual narrative

The pilot report that after a normal takeoff and landing gear retraction, he began to level the airplane at 4,500 ft above ground level when the left engine began to run rough. The pilot and pilot-rated passenger then reduced power on the left engine until the roughness abated and agreed that they should return to the departure airport. While on the downwind leg of the traffic pattern, the pilot placed the landing gear handle in the down position, but the landing gear down indication light did not illuminate. The pilot and pilot-rated passenger attempted to troubleshoot the issue before the pilot ultimately decided to attempt a manual extension of the landing gear. The pilot rated passenger then continued manual extension and was able to turn the crank approximately 50 times before it would no longer turn, and he believed it was “against the stops.” The pilot still did not observe an indication that the landing gear were extended, but decided that they needed to land as a result of the difficulty in maintaining altitude and airspeed. After touchdown on the main landing gear the nose of the airplane settled onto the runway and the airplane skidded to a stop. A bulkhead in airplane’s fuselage structure was substantially damaged during the landing. Following the accident, maintenance personnel examined the airplane and reported that their initial attempts to extend the landing gear normally were unsuccessful. After they “tapped the [landing gear] relay with a hammer” the landing gear extended and retracted normally during several test attempts. The landing gear were also successfully extended manually after the manual extension crank was turned about 10 additional times beyond where it was found following the accident. Additionally, examination of the left engine identified two oil-fouled spark plugs as likely contributors to the engine roughness reported during the accident flight. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft systems-Landing gear system-Gear extension and retract sys-Malfunction

Verbatim from NTSB's published report. Source file NTSB_2024_ERA24LA307.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗