NTSB CAROL · Event
Event FTW92IA009
Aircraft involved
Probable cause & findings
THE PARTIAL DISCONNECTION OF THE ELECTRICAL CONNECTOR AT THE TORQUE SENSING UNIT.
Factual narrative
DURING THE TAKEOFF ROLL, THE PILOT OBSERVED THE TORQUE INDICATIONS OF THE RIGHT ENGINE DROP TO 80 PERCENT AND THE FIRE WARNING LIGHT FOR THE SAME ENGINE ILLUMINATE. THE PILOT ABORTED THE TAKEOFF AND DEPLANED THE PASSENGERS. AIRCRAFT FIRE AND RESCUE PERSONNEL EXTINGUISHED THE FIRE IN THE RIGHT ENGINE. A TEARDOWN AND ANALYSIS OF THE RIGHT ENGINE REVEALED THAT THE ELECTRICAL CONNECTOR OF THE TORQUE SENSING UNIT BECAME LOOSE. THE LOOSE CONNECTION RESULTED IN EXCESS FUEL BEING DUMPED IN THE ENGINE CAUSING A POOLING FIRE. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_1991_FTW92IA009.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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