NTSB CAROL · Event
Event FTW98LA007
Aircraft involved
Probable cause & findings
Inadequate maintenance which resulted in diminished carburetor heat effectiveness due to missing alternate air doors. Contributing were conducive carburetor icing weather conditions, low ceilings during the emergency descent, and the lack of suitable terrain for the forced landing.
Factual narrative
On October 6, 1997, at 1830 central daylight time, a Beech G18S airplane, N9312Y, owned and operated by May Air Express of New Boston, Texas, was substantially damaged during a forced landing following a loss of engine power, near Crosbyton, Texas. The airline transport rated pilot, the sole occupant, sustained serious injuries. Instrument meteorological conditions prevailed in the vicinity of the accident and an IFR flight plan was filed for the Title 14 CFR Part 135 air cargo flight. The flight originated from Lubbock Municipal Airport, Lubbock, Texas, at 1730. The pilot reported the following information in the Pilot/Operator Aircraft Accident Report(NTSB Form 6120.1/2) and during an interview with a FAA inspector. He stated that, while in cruise flight at 9,000 feet MSL, the left engine began to "run rough and lose power," which he suspected to be due to "carburetor ice." He further stated that he "deployed the manifold heat" but "encountered mechanical trouble moving the lever all the way down (heat on)." After " a few minutes" the he secured the left engine and feathered the propeller to "let the ice melt." He "repeatedly" attempted to restart the engine, but the propeller "would not unfeather." During the "whole ordeal" the pilot was unable to maintain altitude or a descent rate less than "200 feet per minute," and the aircraft kept buffeting on the edge of a stall. He stated that, after the airplane descended through a scattered cloud layer, he realized that he would not make it to the Crosbyton Airport. Subsequently, he executed a forced landing to grass covered terrain in a canyon about 5 miles northeast of the airport. He reported that the touch down was "hard but smooth [and then the airplane] struck uneven ground." According to recorded transmissions between the pilot and Lubbock Approach Control, the pilot notified the controller at Lubbock Approach that the airplane was experiencing a problem involving "manifold icing," and he would be landing at Crosbyton Municipal Airport, Crosbyton, Texas. Examination of the aircraft by an FAA airworthiness inspector found that the front of the airplane, from the instrument panel forward, was separated from the fuselage. Both engine nacelles were found separated from the wings and the empennage and tail remained intact. He reported that the hinge for the alternate air door on the left engine was attached, but the alternate air door(part number, 18-970011-25) was missing. He stated that the hinge did not appear to be damaged or distorted. The alternate air door was not found in the wreckage. Examination of the right engine revealed that the alternate air door was also missing from its hinge (which was not damaged). According to the FAA airworthiness inspector, a missing alternate air door on the carburetor air box would allow ambient air to enter the carburetor, rendering the carburetor heat system ineffective. At the time of the accident the reported weather conditions at the Lubbock Airport, located 32 nautical miles west of the accident site were; winds from 140 degrees at 15 knots, a scattered cloud layer at 800 feet, a broken cloud layer at 1,600 feet, and an overcast cloud layer at 11,000 feet. The temperature was 64 degrees and the dew point was 63 degrees. According to carburetor icing probability charts, the reported temperature and dew point values would be favorable to the formation of induction system icing. According to the Pilot/Operator Aircraft Accident Report(NTSB form 6120.1/2) the airline transport rated pilot had accumulated a total of 3,222 hours, of which 1,328 hours were in the Beech 18. The pilot had accumulated 650 hours of night flight time, of which 180 hours were in the Beech 18. While in cruise flight at 9,000 feet MSL, the left engine began to 'run rough and lose power.' The pilot said he interpreted the problem as carburetor icing and applied carburetor heat. With the engine still running rough, the left propeller was feathered and the left engine shut down. Restart attempts were not successful. Unable to maintain altitude, the pilot requested to land at a nearby airport. After descending through IMC weather, the pilot realized that he would not make it to the airport, and executed a forced landing to rough/uneven terrain. Examination of the engines revealed that the alternate air doors were missing on the right and left engine. The hinges for the doors were attached to both carburetors and showed no evidence of distortion or impact damage. The doors were not found at the wreckage site. A missing alternate air door would allow ambient air to enter the carburetor, rendering the carburetor heating system ineffective. According to carburetor icing probability charts, the reported temperature and dew point values would be favorable to the formation of induction system icing. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_1997_FTW98LA007.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (icing, stall, imc, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
- Embry-Riddle Scholarly Commons 2023 · Faculty research project
Reconfigurable Guidance and Control Systems for Emerging On-Orbit Servicing, Assembly, and Manufacturing (OSAM) Space Vehicles
Dynamic response to emergent situations is a necessity in the on-orbit servicing, assembly, and manufacturing (OSAM) field, because traditional on-orbit guidance and control (G&C) cannot respond effic…
- arXiv 2023 · arXiv preprint
Variation of Critical Crystallization Pressure for the Formation of Square Ice in Graphene Nanocapillaries
Two-dimensional square ice in graphene nanocapillaries at room temperature is a fascinating phenomenon and has been confirmed experimentally.
- Embry-Riddle Scholarly Commons 2023 · Conference paper
The Value of Strong Partnerships to Build a Successful Aviation Maintenance Career Pathway Program for Transitioning Military Service Members
The aerospace industry is competing with other industries for a qualified workforce, and many of those competing industries are investing heavily in creating workforce development pipelines.
- arXiv 2022 · arXiv preprint
Enhanced Prediction of Three-dimensional Finite Iced Wing Separated Flow Near Stall
Icing on three-dimensional wings causes severe flow separation near stall. Standard improved delayed detached eddy simulation (IDDES) is unable to correctly predict the separating reattaching flow due…
- NASA NTRS 2019 · Contractor Report (CR)
An Evaluation of an Analytical Simulation of an Airplane with Tailplane Icing by Comparison to Flight Data
This report presents the assessment of an analytical tool developed as part of the NASA/FAA Tailplane Icing Program. The analytical tool is a specialized simulation program called TAILSM4 which was de…
- NASA NTRS 2019 · Technical Publication (TP)
NASA/FAA Tailplane Icing Program: Flight Test Report
This report presents results from research flights that explored the characteristics of an ice-contaminated tailplane using various simulated ice shapes attached to the leading edge of the horizontal …
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