NTSB CAROL · Event
Event LAX04CA303
Registry · N54RR
FAA Aircraft Registry record.
Make / Model
ROCKWELL INTERNATIONAL 112TC
Year of manufacture
1976 · 28 years old at event
Engine
LYCOMING I0360 SER (180 hp)
Seats / Engines
4 seats · 1 engine
Last airworthiness date
19761008
ADS-B equipped
Yes — Mode-S A6D71A
Registrant of record
VALENTIN JOSE E
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
the pilot's failure to extend the landing gear prior to landing. Factors in the accident were the pilot's failure to use a checklist and to verify that the gear were extended.
Factual narrative
On August 16, 2004, about 0915 mountain standard time, a Rockwell Commander 112TC, N54RR, landed gear up at Laughlin/Bullhead International Airport, Bullhead City, Arizona. The pilot/owner was operating the airplane under the provisions of 14 CFR Part 91. The private pilot, the sole occupant, was not injured; the airplane sustained substantial damage. Visual meteorological conditions prevailed, and a flight plan had not been filed. The personal cross-country flight originated from Henderson Executive Airport, Las Vegas, Nevada, about 0835 Pacific daylight time, with a planned destination of Bullhead City. In a telephone conversation with a National Transporation Safety Board investigator, the pilot reported that he was attempting to land on runway 16. In an effort to make the approach faster, he opted to leave the landing gear retracted for the initial approach. He mentally preformed a prelanding checklist "GUMPS," which included checking the gas, undercarriage, mixture, and propeller. During the landing flare, the airplane touched down on the bottom of the fuselage, and the pilot realized that he had forgotten to extend the landing gear. The pilot further stated that he did not use a physical checklist prior to landing. He also noted that he did not hear the gear warning horn sound, which he thought was a result of using external noise cancellation headsets. The pilot reported no mechanical malfunctions or failures with the airplane prior to impact. The accident was upgraded from an incident on August 24, 2004. The airplane incurred damage to the wing carry-though spar and possibly the fuselage aft bulkhead. The airplane landed gear up. In an effort to make the approach faster, the pilot opted to leave the landing gear retracted for the initial approach. During the landing flare, the airplane touched down on the bottom of the fuselage, and the pilot realized that he had forgotten to extend the landing gear. The pilot further stated that he did not use a physical checklist prior to landing. The pilot reported no mechanical malfunctions or failures with the airplane prior to impact. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12
Verbatim from NTSB's published report. Source file
NTSB_2004_LAX04CA303.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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