Skip to content

Atlas / NTSB / MIA88LA018

NTSB CAROL · Event

Event MIA88LA018

1987-10-24 KEY COLONY BCH., Florida, United States None 1 aircraft Status: Completed

Aircraft involved

Factual narrative

THE PLT STATED THAT HE DID NOT CHECK THE FUEL SYSTEM FOR CONTAMINATES AFTER REFUELING BUT AN EIGHTEEN MINUTE FLT AFTER REFUELING WAS UNEVENTFUL. HE THEN LANDED THE HELICOPTER, REMAINED ON THE GROUND APRX 20 MINUTES, PERFORMED A WALK AROUND INSP, AGAIN WITHOUT CHECKING THE FUEL SYSTEM, THEN DEPARTED ON A SIGHTSEEING FLT ALONG THE SHORELINE. WHILE IN CRUISE FLT AT APRX 500 FT THE ENG QUIT. AN AUTOROTATIVE LANDING IN THE WATER WAS PERFORMED WITH NO DAMAGE TO THE HELICOPTER BUT THE PLT THEN ROLLED IT TO THE RT TO STOP THE ROTATION OF THE BLADES TO EXIT FROM ACFT. THE HELICOPTER WAS SUBSTANTIALLY DAMAGED. ACCORDING TO A MECHANIC THE ENG QUIT DUE TO WATER AND FUEL CONTAMINATION. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1987_MIA88LA018.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (fuel contamination). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗