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Atlas / NTSB / NYC04LA183

NTSB CAROL · Event

Event NYC04LA183

2004-08-03 Cooperstown, New York, United States Airport · K23 Serious 1 aircraft Status: Completed

Aircraft involved

Probable cause & findings

The pilot's failure to maintain adequate airspeed and her premature rotation which resulted in an inadvertent stall/mush and subsequent impact with the ground.

Factual narrative

On August 3, 2004, at 1455 eastern daylight time, N7957U, a Cessna 172F, was substantially damaged when it impacted the runway, during takeoff from the Cooperstown-Westville Airport (K23), Cooperstown, New York. The certificated commercial pilot was seriously injured. Visual meteorological conditions prevailed and no flight plan was filed for the local personal flight conducted under 14 CFR Part 91. According to the pilot, she initiated the takeoff from runway 20 (a 2,600-foot long, 125-ft. wide turf runway), and during the takeoff roll, the airplane veered sharply to the left. She applied right rudder to realign the airplane on the centerline, and when "nothing changed," she "responded instinctively" and pulled back on the controls to lift the airplane off the runway. Because the airplane "lacked adequate airspeed," immediately after rotation, it descended, and impacted the ground. The pilot additionally stated that the correct action, to "pull the power back" and abort the takeoff, did not occur to her until it was too late. Examination of the airplane by the FAA inspector revealed substantial damage to the empennage of the airplane. No mechanical deficiencies were observed. The winds reported at an airport approximately 38 miles to the northwest, at 1456, were from 260 degrees at 3 knots. During the takeoff roll, the airplane veered sharply to the left. The pilot applied right rudder to realign the airplane on the centerline, and when the airplane did not respond, she "instinctively" pulled back on the controls to lift the airplane off the runway. Because the airplane "lacked adequate airspeed," immediately after rotation, it descended, and impacted the ground. The pilot stated that the correct action, "to pull the power back" and abort the takeoff, did not occur to her until it was too late. No mechanical deficiencies were observed with the airplane. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_2004_NYC04LA183.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗