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Atlas / NTSB / SEA99LA073

NTSB CAROL · Event

Event SEA99LA073

1999-05-23 BREMERTON, Washington, United States Airport · PWT None 1 aircraft Status: Completed

Registry · N2567K

FAA Aircraft Registry record.

Make / Model

CESSNA 180K

Year of manufacture

1978 · 21 years old at event

Engine

CONT MOTOR O-470 SERIES (230 hp)

Seats / Engines

4 seats · 1 engine

Last airworthiness date

19780803

ADS-B equipped

Yes — Mode-S A2711F

Registrant of record

BRYANT KENNETH D

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

Failure of the landing gear attach bolt due to fatigue failure resulting in the left main landing gear collapsing.

Factual narrative

On May 23, 1999, approximately 1535 Pacific daylight time, a Cessna 180K, N2567K, impacted the runway at Bremerton National Airport, Bremerton, Washington, after the failure of a main gear leg during the landing roll. The private pilot, who was the operator of the aircraft, was not injured, but the aircraft sustained substantial damage. The 14 CFR Part 91 flight, which departed Crest Airpark, Covington, Washington, about 30 minutes earlier, was being operated in visual meteorological conditions. No flight plan had been filed, and there was no report of an ELT activation. According to the pilot, who was performing a wheel landing, the touchdown was normal. But as the landing roll continued, he lost control of the aircraft when the left main gear leg failed. Immediately after the gear failed, the aircraft settled onto the runway and slid to a stop. Post-accident inspection revealed that the attachment bolt from the gear leg broke in two pieces. The bolt was sent to the National Transportation Safety Board Materials Laboratory, Washington D.C. for examination. The specialist reported that "the bolt separated at the edge of the self-locking nut, through the first thread on the shank." Further examination with the aid of a low-power binocular microscope revealed three major fracture zones. The specialist reported that two of the zones were "fairly flat and propagated on a plane that was roughly perpendicular to the bolt axis, typical of fatigue progression." One of the zones was covered with heavy accumulation of oxides and corrosion deposits. The other zone was free of oxidation and deposits. The third zone displayed a fracture propagation on a slant (45 degree) plane. The specialist reported this zone as "typical of a final overstress separation." The specialist reported that "the fatigue occupied approximately 75 percent of the bolt cross section at the fracture location." The specialist also reported that the presence of oxide and corrosion deposits suggest an "old crack." There was no evidence found of thread stripping. The aircraft was purchased new in 1978. The aircraft maintenance logbooks indicate that that the aircraft had accumulated about 38 hours of total time at the annual inspection performed in March of 1981. The next annual inspection was signed off in June 1995, with a total time still indicating 38 hours. In February 1999, the logbook indicated an annual inspection with a total time of 69.5 hours accumulated. The pilot reported a total aircraft time of 77 hours at the time of the accident. The pilot reported that he performed a normal wheel landing. During the landing roll, the left main gear leg failed. Post-accident inspection revealed that the attachment bolt from the gear leg broke in two pieces. During the metallurgical examination, the specialist found that three major fracture zones were present. Two of the zones were fairly flat and propagated on a plane that was perpendicular to the bolt axis, typical of fatigue progression. One of the zones was covered with heavy accumulation of oxides and corrosion deposits. The other zone was free of oxidation and deposits. The third zone displayed a fracture propagation on a 45 degree slant. This zone was typical of a final overstress separation. The fatigue zones occupied about 75 percent of the bolt cross section at the fracture location. The specialist reported that the presence of oxide and corrosion deposits suggested an 'old crack.' There was no evidence found of thread stripping. Maintenance records indicate that since the time of manufacture in 1978, the aircraft had accumulated a total time of 77 hours. During this time, there were several years in which the aircraft had not been operated. Source: NTSB Aviation Accident Database (Pre-2008 Archive) Retrieved: 2026-02-12

Verbatim from NTSB's published report. Source file NTSB_1999_SEA99LA073.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.

Related research

What the literature says.

Academic papers and agency reports matching this event's aircraft type or causal vocabulary (maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.

Browse the full corpus — academia portal ↗