NTSB CAROL · Event
Event WPR13FA243
Aircraft involved
Probable cause & findings
Fatigue failure of the six bolts that secured the bevel gear to the first stage planetary carrier, which caused the transmission to seize while the helicopter and main rotor were still operating.
Factual narrative
HISTORY OF FLIGHTOn May 25, 2013, about 1745 Pacific daylight time, a Hiller UH-12E, N99090, landed hard after the main rotor head assembly separated from the helicopter at Pangborn Memorial Airport (EAT), Wenatchee, Washington. The commercial pilot was not injured, and the passenger sustained minor injuries. The helicopter sustained substantial damage throughout. The helicopter was registered to and operated by the pilot under the provisions of 14 Code of Federal Regulations Part 91. No flight plan was filed for the personal flight. Visual meteorological conditions prevailed for the flight that originated from EAT at about 1730 hours. The pilot reported that after takeoff, when he was about three miles away from the airport, he heard a noise above and behind him. The pilot immediately turned the helicopter back towards the airport; when about one mile away, he heard a second noise. The pilot continued to the airport and hovered about four feet above the ground; the main rotor head and blades separated from the helicopter and flew up into the air. Subsequently, the helicopter impacted the ground hard and the tailboom separated about mid span. Shortly thereafter, the main rotor head and blades impacted the ground about 300 feet away. PERSONNEL INFORMATIONThe pilot, age 61, held a commercial pilot certificate for single- and multi-engine land airplane, helicopter, and a certified flight instructor certificate for helicopter issued June 10, 2012. The pilot also held an airplane instrument rating. On July 6, 2012, he was issued a second-class airman medical certificate with the limitation that he must wear corrective lenses, and possess glasses for near and intermediate vision. The pilot reported that at the time of the accident he had about 1,555 total hours, 928 of which were in the accident helicopter make and model. AIRCRAFT INFORMATIONThe three seat, high skid helicopter, serial number 1395, was manufactured in 1962. It was powered by a Lycoming VO-540-C2A 305-horsepower engine. The helicopter's most recent maintenance inspection was a 100 hour inspection that occurred on November 1, 2012 at an airframe total time of 10,568. METEOROLOGICAL INFORMATIONAt 1755, weather at EAT was reported as wind from 080 degrees at 5 knots, visibility of 10 statute miles, broken clouds at 10,000 feet above ground level, temperature 18 degrees C, dewpoint 3 degrees C, and an altimeter setting of 29.93"Hg. AIRPORT INFORMATIONThe three seat, high skid helicopter, serial number 1395, was manufactured in 1962. It was powered by a Lycoming VO-540-C2A 305-horsepower engine. The helicopter's most recent maintenance inspection was a 100 hour inspection that occurred on November 1, 2012 at an airframe total time of 10,568. WRECKAGE AND IMPACT INFORMATIONDue to the nature of the accident, the NTSB did not conduct an on scene investigation. However, it was reported by airport management that the helicopter's main fuselage was mostly intact and sustained minimal damage. The landing skids exhibited no apparent deformation. The tailboom was fracture separated about midspan, however, the tail rotor drive shaft was still connected along the entire length. The main rotor hub and blades separated from the main rotor shaft and came to rest about 300 feet away from the fuselage. TESTS AND RESEARCHPostaccident Examination The main transmission remained attached to the helicopter. The main transmission housing exhibited multiple fractures on its center (second stage planetary gear) housing; the fractures were primarily orientated vertically, and were through the thin walled section of the housing. The main rotor shaft and tail rotor drive shaft were still connected to the transmission. After disconnecting the tail rotor drive shaft from the main transmission, investigators attempted to rotate the main rotor shaft by hand; however, it would not turn clockwise or counterclockwise. The main rotor shaft fracture surface was removed from the main rotor shaft for further examination. The tail rotor drive assembly was removed from the main transmission lower housing; metallic chips and flakes were observed in the residual oil and on the gear teeth. One of the pieces appeared to have heat discoloration. The main transmission was removed from the helicopter for further examination. Transmission Teardown The transmission was removed and examined at the facilities of Hiller Aircraft Corporation. The transmission was disassembled; substantial damage was observed to the first stage planetary (epicyclic) gear teeth and the input gear teeth. A high quantity of metallic chips and flakes were discovered at the bottom of the lower housing and throughout the first stage planetary assembly. All six bolts securing the bevel gear to the first stage planetary carrier were fractured. Only one of the six separated bolt heads remained secured with safety wiring; the remaining five bolt heads were not found. Inspection of the oil supply lines and nozzles found no evidence of blockages, and the transmission's internal components above the first stage planetary assembly showed no signs of oil starvation. The center housing, bevel gear, fractured bevel gear bolt, and the fracture surface of the main rotor shaft were retained for metallurgical examination at the NTSB materials laboratory. NTSB Materials Laboratory The NTSB materials lab removed and cleaned the six bolts from the bevel gear. All of the bolt fracture surfaces exhibited comparable features. Each bolt exhibited fatigue fracture features, such as crack arrest and beach marks that surrounded a center region consistent with overstress. The fatigue cracks initiated along the thread roots of the bolts; these cracks were generally positioned about 180 degrees from each other, and were consistent with failure from reverse bending fatigue. The transmission center housing was examined and contained three longitudinal cracks, each of which was present across a bolt hole in the flange. The three cracks progressed through most of the housing cross section to the opposite flange. Two of the cracks were backcut, and the crack faces were analyzed. The crack faces exhibited features consistent with overstress fracture from radial stresses (hoop stresses); there were no indications of corrosion or progressive failure modes. The portion of main rotor shaft that was previously sectioned about two inches from the fracture surface was analyzed. The fracture surface of the shaft was orientated 45 degrees from the longitudinal direction of the shaft, and was generally dark and exhibited a rough texture. The shaft had also been deformed to one side; all of these features were consistent with overstress failure in tension. The pilot reported that, after takeoff, when he was 3 miles from the airport, he heard a noise above and behind him. The pilot immediately turned the helicopter back toward the airport; when about 1 mile away, he heard a second noise. The pilot continued to the airport and was hovering the helicopter about 4 feet above the ground when the main rotor head and blades separated from the helicopter, flew up into the air, and impacted the ground about 300 feet away. The helicopter impacted the ground hard, and the tailboom separated about midspan. Postaccident examination revealed that the main transmission housing exhibited multiple fractures on its second stage planetary gear housing; the fractures were primarily orientated vertically and were through the thin-walled section of the housing. Analysis of these fracture surfaces revealed that the cracks were consistent with overstress from radial stresses. The transmission was disassembled and substantial damage was observed to the first stage planetary gear teeth and the input gear teeth. A high quantity of metallic chips and flakes were discovered at the bottom of the lower housing and throughout the first stage planetary assembly. All six bolts securing the bevel gear to the first stage planetary carrier were fractured. Only one of the six separated bolt heads remained secured with safety wiring. The six bolts were removed each bolt exhibited fatigue fracture features consistent with overstress, such as crack arrest and beach marks, that surrounded a center region. The fatigue cracks initiated along the thread roots of the bolts; these cracks were generally positioned about 180 degrees from each other, and were consistent with failure from reverse bending fatigue. After the bolts fractured, the bevel gear was unconstrained, leading to overstress fracture of the adjacent components. The fracture surface of the main rotor shaft was analyzed; the fracture surface was orientated 45 degrees from the longitudinal direction of the shaft, and the shaft was deformed to one side. All features were consistent with overstress failure in tension. A complete set of maintenance records were not available for review, thus, it could not be determined if the bolts met installation requirements or if regular inspection of bolt tightness was met. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- C Aircraft-Aircraft propeller/rotor-Main rotor system-(general)-Fatigue/wear/corrosion - C
- C Aircraft-Aircraft power plant-(general)-(general)-Fatigue/wear/corrosion - C
- C Aircraft-Fluids/misc hardware-Misc hardware-(general)-Not specified - C
Verbatim from NTSB's published report. Source file
NTSB_2013_WPR13FA243.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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Related research
What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (stall, maintenance). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
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