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Atlas / NTSB / WPR15LA038

NTSB CAROL · Event

Event WPR15LA038

2014-11-07 Bullhead City, Arizona, United States Airport · KIFP None 1 aircraft Status: Completed

Registry · N9578X

FAA Aircraft Registry record.

Make / Model

CESSNA 210B

Engine

CONT MOTOR I0-470 SERIES (260 hp)

Seats / Engines

4 seats · 1 engine

ADS-B equipped

Yes — Mode-S AD522E

Registrant of record

TVAT LLC

Source: FAA Aircraft Registry (releasable master file).

Aircraft involved

Probable cause & findings

The failure of the landing gear actuator housing during landing for reasons that could not be determined based on the available evidence.

Factual narrative

On November 7, 2014, at 1730 mountain standard time, a Cessna 210B, N9578X, experienced a landing gear malfunction after takeoff from Laughlin/Bullhead International Airport, Bullhead City, Arizona. Tristate Careflight LLC operated the airplane under the provisions of 14 Code of Federal Regulations, Part 91. The commercial pilot and three passengers were uninjured, and the airplane sustained substantial damage to the horizontal stabilizer during the landing. Visual meteorological conditions prevailed, and no flight plan had been filed. The pilot stated that after takeoff he heard a loud bang after he moved the landing gear handle to the UP position. The landing gear indication lights were not illuminated. He cycled the landing gear handle, which had no effect. He also determined that the flaps would not operate. During a low pass the tower informed the pilot that the landing gear were in a transit position (not retracted, not locked down). The pilot attempted to execute the emergency gear extension procedure, which was not successful. During the landing the gear completely collapsed, the airplane slid to a stop on its belly and tipped to the left, damaging the left horizontal stabilizer. The pilot reported that an airframe and power plant mechanic visually examined the landing gear actuator, and stated that the actuator housing had split, allowing the loss of hydraulic system pressure. No further examination was accomplished and the reason for the housing failure was not determined. The pilot stated that, after takeoff, he heard a loud bang after he moved the landing gear handle to the "up" position. The landing gear indication lights did not illuminate. He cycled the landing gear handle, which had no effect. In addition, the flaps would not operate. During a low pass, the tower controller informed the pilot that the landing gear were in a transit position (not retracted, not locked down). The pilot attempted to execute the emergency gear extension procedure; however, the gear would not extend. During the landing, the gear completely collapsed, and the airplane slid to a stop on its belly and then tipped on its left side, which resulted in damage to the left horizontal stabilizer. The pilot reported that an airframe and powerplant mechanic visually examined the landing gear actuator and stated that the actuator housing had split, which resulted in the loss of hydraulic system pressure. However, no further examinations were conducted, and the reason for the housing failure could not be determined. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12

NTSB Findings

Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).

  • Aircraft-Aircraft systems-Landing gear system-Landing gear actuator-Failure
  • C Not determined-Not determined-(general)-(general)-Unknown/Not determined - C

Verbatim from NTSB's published report. Source file NTSB_2014_WPR15LA038.txt. Findings + structured fields enriched from FAA avall.mdb. Full investigation docket on data.ntsb.gov ↗.