NTSB CAROL · Event
Event WPR23LA077
Registry · N65Y
FAA Aircraft Registry record.
Make / Model
BEECH V35B
Year of manufacture
1977 · 45 years old at event
Engine
CONT MOTOR IO 520 SERIES (285 hp)
Seats / Engines
6 seats · 1 engine
Last airworthiness date
19771111
ADS-B equipped
Yes — Mode-S A88C87
Registrant of record
LIPPMAN THOMAS N TRUSTEE
Source: FAA Aircraft Registry (releasable master file).
Aircraft involved
Probable cause & findings
The pilot’s inadvertent use of the mixture control instead of the throttle, which resulted in fuel starvation and the subsequent loss of engine power.
Factual narrative
On December 24, 2022, about 1653 Pacific standard time, a Beech V35B, N65Y, was substantially damaged when it was involved in an accident near Livermore Municipal Airport (LVK), Livermore, California. The pilot was seriously injured. The airplane was operated as a Title 14 Code of Federal Regulations Part 91 personal flight. The pilot reported that he departed runway 7L at LVK with the intention of remaining within the airport traffic pattern. While on the upwind leg of the traffic pattern, the cabin door opened, and he slowed the airplane down “using the throttle.” He stated that due to the wind noise, he could not hear the tower controller well and that he could not see the instruments but could see the engine control knobs. The pilot then heard the tower controller say “climb, climb, climb,” and at that time, the pilot realized the airplane was descending toward a building. The pilot stated that he “pushed the throttle in” but the airplane continued to descend and impacted a building. The pilot added that he usually takes off with the mixture full rich, the propeller full forward, and the throttle at full. When he slowed the airplane, he “slowed it with the throttle.” Due to the dark conditions, he could not be sure if he mistakenly pulled the mixture control knob to slow the airplane down. A witness, located near the accident site, reported that they heard the accident airplane’s engine sputtering as it passed by his location, followed by the sound of the airplane impacting a building. Examination of the recovered wreckage revealed no preaccident mechanical malfunctions or failures with the airplane that would have precluded normal operation. Fuel expelled from various fuel lines when they were removed. The engine-driven fuel pump was removed, and the drive shaft was found intact. The fuel pump drive shaft rotated freely by hand. The fuel pump was disassembled and found to be unremarkable. Continuity of the throttle, propeller, and mixture controls was established from the cockpit to their respective control arms and moved from stop to stop by hand. Examination of the engine controls in the cockpit revealed the throttle knob was about 1 inch from full forward, the mixture was about 2 inches from full forward, and the propeller lever was about 1/2 inch from full forward. The pilot planned on remaining in the traffic pattern for night flight. Shortly after takeoff, while on the upwind leg of the traffic pattern, the cabin door opened; the pilot stated that he slowed the airplane by using the throttle. He added that it was dark and that he could not see the instruments, but he could see the engine control knobs. The pilot realized the airplane was descending toward a building when he heard the tower controller say “climb, climb, climb.” The pilot then “pushed the throttle in.” The airplane continued to descend and impacted a building. Additionally, the pilot added that due to the dark conditions, he may have mistakenly pulled the mixture control knob to slow the airplane down instead of using the throttle. Postaccident examination of the airframe and engine revealed no evidence of mechanical malfunctions or failures that would have precluded normal operation. Continuity of the throttle, propeller, and mixture controls was established from the cockpit to their respective control arms. Examination of the throttle revealed the throttle knob was about 1 inch from full forward, the mixture control was about 2 inches from full forward, and the propeller controller lever was about ½ inch from full forward. The pilot likely inadvertently manipulated the mixture to a lean position instead of the pulling back on the throttle, which resulted in the reduction of engine power. Source: NTSB Aviation Accident Database Retrieved: 2026-02-12
NTSB Findings
Hierarchical cause / factor breakdown from the FAA bulk avdata database. Each finding tagged C (Cause) or F (Factor).
- — Personnel issues-Task performance-Use of equip/info-Use of equip/system-Pilot
- — Aircraft-Aircraft power plant-Engine controls-Mixture control-Unintentional use/operation
Verbatim from NTSB's published report. Source file
NTSB_2022_WPR23LA077.txt.
Findings + structured fields enriched from FAA avall.mdb.
Full investigation docket on
data.ntsb.gov ↗.
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What the literature says.
Academic papers and agency reports matching this event's aircraft type or causal vocabulary (fuel starvation). Sourced from NASA NTRS, NTSB Safety Studies, FAA CAMI, AOPA Air Safety Institute, Embry-Riddle Scholarly Commons, arXiv, and the Semantic Scholar academic graph.
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